HL incident on 2016-09-05 — TX

Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-09-05 13:45
Report number
Location
TX
Narrative
On 9/5/2016 an kinder morgan employee noticed a leak on the seal of the pump used for tank 80-11. The pump was shut down and the seal replaced. The product was recovered and the contaminated soil was remediated.
Detailed record list
Report Received Date
2016-10-05 00:00:00
Iyear
2016
Report Number
20160319
Supplemental Number
21744
Report Type
Original Final
Operator Id
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-09-05 13:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
16
Recovered Bbls
16
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2016-09-05 13:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-09-05 13:45:00
Restart Datetime
2016-09-05 16:00:00
On Site Datetime
2016-09-05 14:00:00
Nrc Rpt Datetime
2016-09-05 14:28:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal
Segment Name
Tank 80-11
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
1974
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1400
Est Cost Prop Damage
0
Est Cost Emergency
27700
Est Cost Environmental
27300
Est Cost Other
0
Prpty
56400
Accident Psig
27
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak unrelated to controller's actions
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear And Tear
Preparer Name
D******* S*******
Preparer Title
Director Compliance Codes And Standards
Preparer Email
D****************@k***********.com
Preparer Telephone
7134206496
Prepared Date
2016-10-05 00:00:00
Authorizer Name
D******* S*******
Authorizer Telephone
7134206496
Authorizer Title
Director Compliance Codes And Standards
Authorizer Email
D****************@k***********.com
Narrative
On 9/5/2016 an kinder morgan employee noticed a leak on the seal of the pump used for tank 80-11. The pump was shut down and the seal replaced. The product was recovered and the contaminated soil was remediated.
Report Received Date 2016-10-05 00:00:00
Iyear 2016
Report Number 20160319
Supplemental Number 21744
Report Type Original Final
Operator Id 26041 PHMSA Enforcement
Name Kinder Morgan Liquid Terminals, Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-09-05 13:45:00
Location Latitude 29.72979 Google Maps OpenStreetMap
Location Longitude -95.22212 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 16
Recovered Bbls 16
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2016-09-05 13:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-09-05 13:45:00
Restart Datetime 2016-09-05 16:00:00
On Site Datetime 2016-09-05 14:00:00
Nrc Rpt Datetime 2016-09-05 14:28:00
Nrc Rpt Num 1158205 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Galena Park Terminal
Segment Name Tank 80-11
Onshore State Abbreviation Tx
Onshore Postal Code 77547
Onshore City Name Galena Park
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 1974
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1400
Est Cost Prop Damage 0
Est Cost Emergency 27700
Est Cost Environmental 27300
Est Cost Other 0
Prpty 56400
Accident Psig 27
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak unrelated to controller's actions
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Wear And Tear
Preparer Name D******* S*******
Preparer Title Director Compliance Codes And Standards
Preparer Email D****************@k***********.com
Preparer Telephone 7134206496
Prepared Date 2016-10-05 00:00:00
Authorizer Name D******* S*******
Authorizer Telephone 7134206496
Authorizer Title Director Compliance Codes And Standards
Authorizer Email D****************@k***********.com
Narrative On 9/5/2016 an kinder morgan employee noticed a leak on the seal of the pump used for tank 80-11. The pump was shut down and the seal replaced. The product was recovered and the contaminated soil was remediated.

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