HL incident on 2016-08-16 — TX

Operator
Dixie Pipeline Company Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-08-16 00:22
Report number
Location
TX
Narrative
At approximately 12:22 am cdt on august 16, 2016, enterprise control center received hazardous gas esd for both opelika station and opelika terminal. At 12:23 am motor operated mainline valves upstream and downstream of the station were closed. Local operations arrived on site at and confirmed the leak at 12:55 am. With the help of emergency responders, highway 51 was closed to traffic on the north and south side of the station. Station was isolated and blown down, and leak was confirmed to be originating from station strainer. Strainer o-ring was identified as having failed and new o-ring was installed in strainer. At 10:40 am, station was restarted and resumed normal operations. Upon further investigation, leak was determined to have started at 10:00 pm the night before, and a total of 6.91 bbls of propane was released. There were no injuries, evacuations, or fire as a result of this release. In lieu of performing the o-ring analysis, the strainer was removed and a spool piece with a cone strainer was installed in its place on september 11, 2016.
Detailed record list
Report Received Date
2016-09-13 00:00:00
Iyear
2016
Report Number
20160296
Supplemental Number
21943
Report Type
Supplemental Final
Operator Id
Name
Dixie Pipeline Company Llc
Operator Street Address
1100 Louisiana St.
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-08-15 22:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
6.91
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2016-08-16 00:22:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-08-16 00:23:00
Restart Datetime
2016-08-16 10:40:00
On Site Datetime
2016-08-16 00:55:00
Nrc Rpt Datetime
2016-08-16 01:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Opelika Station
Segment Name
Line Id 120
Onshore State Abbreviation
Al
Onshore Postal Code
36804
Onshore City Name
Opelika
Onshore County Name
Lee
Designated Location
Milepost/valve Station
Designated Name
631.44
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Strainer
Installation Year
1961
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
290
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
5000
Est Cost Other Details
Cost Associated With Failure Analysis Of The O-Ring From Strainer Assembly
Prpty
5290
Accident Psig
407.9
Mop Psig
1406
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unknown - See Part H
Preparer Name
L**** W*******
Preparer Title
Pipeline Compliance Engineer
Preparer Email
L*********@e****.com
Preparer Telephone
713-381-6748
Prepared Date
2016-12-08 00:00:00
Authorizer Name
L**** W*******
Authorizer Telephone
713-381-6748
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
L*********@e****.com
Narrative
At approximately 12:22 am cdt on august 16, 2016, enterprise control center received hazardous gas esd for both opelika station and opelika terminal. At 12:23 am motor operated mainline valves upstream and downstream of the station were closed. Local operations arrived on site at and confirmed the leak at 12:55 am. With the help of emergency responders, highway 51 was closed to traffic on the north and south side of the station. Station was isolated and blown down, and leak was confirmed to be originating from station strainer. Strainer o-ring was identified as having failed and new o-ring was installed in strainer. At 10:40 am, station was restarted and resumed normal operations. Upon further investigation, leak was determined to have started at 10:00 pm the night before, and a total of 6.91 bbls of propane was released. There were no injuries, evacuations, or fire as a result of this release. In lieu of performing the o-ring analysis, the strainer was removed and a spool piece with a cone strainer was installed in its place on september 11, 2016.
Report Received Date 2016-09-13 00:00:00
Iyear 2016
Report Number 20160296
Supplemental Number 21943
Report Type Supplemental Final
Operator Id 3445 PHMSA Enforcement
Name Dixie Pipeline Company Llc
Operator Street Address 1100 Louisiana St.
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-08-15 22:00:00
Location Latitude 32.577172 Google Maps OpenStreetMap
Location Longitude -85.370262 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 6.91
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2016-08-16 00:22:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-08-16 00:23:00
Restart Datetime 2016-08-16 10:40:00
On Site Datetime 2016-08-16 00:55:00
Nrc Rpt Datetime 2016-08-16 01:27:00
Nrc Rpt Num 1156357 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Opelika Station
Segment Name Line Id 120
Onshore State Abbreviation Al
Onshore Postal Code 36804
Onshore City Name Opelika
Onshore County Name Lee
Designated Location Milepost/valve Station
Designated Name 631.44
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Strainer
Installation Year 1961
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 290
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 5000
Est Cost Other Details Cost Associated With Failure Analysis Of The O-Ring From Strainer Assembly
Prpty 5290
Accident Psig 407.9
Mop Psig 1406
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Unknown - See Part H
Preparer Name L**** W*******
Preparer Title Pipeline Compliance Engineer
Preparer Email L*********@e****.com
Preparer Telephone 713-381-6748
Prepared Date 2016-12-08 00:00:00
Authorizer Name L**** W*******
Authorizer Telephone 713-381-6748
Authorizer Title Pipeline Compliance Engineer
Authorizer Email L*********@e****.com
Narrative At approximately 12:22 am cdt on august 16, 2016, enterprise control center received hazardous gas esd for both opelika station and opelika terminal. At 12:23 am motor operated mainline valves upstream and downstream of the station were closed. Local operations arrived on site at and confirmed the leak at 12:55 am. With the help of emergency responders, highway 51 was closed to traffic on the north and south side of the station. Station was isolated and blown down, and leak was confirmed to be originating from station strainer. Strainer o-ring was identified as having failed and new o-ring was installed in strainer. At 10:40 am, station was restarted and resumed normal operations. Upon further investigation, leak was determined to have started at 10:00 pm the night before, and a total of 6.91 bbls of propane was released. There were no injuries, evacuations, or fire as a result of this release. In lieu of performing the o-ring analysis, the strainer was removed and a spool piece with a cone strainer was installed in its place on september 11, 2016.

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