HL incident on 2016-08-08 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$157,000
Incident datetime
2016-08-08 06:12
Report number
Location
TX
Narrative
On the morning of august 8, 2016 delivery from tank 15 was completed at approximately 02:35. Control center received tank creep alarms and contacted field operations personnel to investigate. At approximately 06:25 field personnel discovered release from tank 15 mixer area. Additional field personnel and resources were dispatched to location while tank 15 was pumped out to below tank mixer level to stop release. All free crude oil was recovered via vacuum truck and contaminated soil was remediated on site. Total volume released was 700 barrels. Approximately 250 barrels were recovered. An estimated 145 barrels was entrained in the soil and an estimated 305 barrels volitalized. It was determined in the field that the mixer assembly had failed causing the release of crude oil from the tank. The mixer assembly was removed and sent for 3rd party failure analysis. Analysis concluded that the cause was the failure of the upper c-clip of the mixer motor assembly, causing excessive vibration and ultimate failure of the mixer hinge. Other mixers of same design and manufacturer in the splp system have been inspected and repaired or retrofitted with manufacturer hinge pin replacement kits.
Detailed record list
Report Received Date
2016-09-06 00:00:00
Iyear
2016
Report Number
20160280
Supplemental Number
22427
Report Type
Supplemental Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-08-08 06:12:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
700
Recovered Bbls
395
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2016-08-08 06:12:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Isolated And Pumped Down.
On Site Datetime
2016-08-08 06:25:00
Nrc Rpt Datetime
2016-08-08 08:29:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colorado City Station-Tank 15
Segment Name
23010-26" Colorado City To Wortham
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Hermleigh
Onshore County Name
Scurry
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7900
Est Cost Prop Damage
157000
Est Cost Emergency
50000
Est Cost Environmental
425000
Est Cost Other
0
Prpty
639900
Accident Psig
20
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Controller Did Not Notify Field After Receiving Initial Tank Creep Alarm.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Failure Of Upper Clip On Mixer Hinge Caused It To Laterally Separate Away From The Tank Causing Vibration Which Led To Complete Failure Of The Mixer Hinge Mechanism.
Additional Vibration Ind
Yes
Additional Support Ind
Yes
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2017-06-19 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On the morning of august 8, 2016 delivery from tank 15 was completed at approximately 02:35. Control center received tank creep alarms and contacted field operations personnel to investigate. At approximately 06:25 field personnel discovered release from tank 15 mixer area. Additional field personnel and resources were dispatched to location while tank 15 was pumped out to below tank mixer level to stop release. All free crude oil was recovered via vacuum truck and contaminated soil was remediated on site. Total volume released was 700 barrels. Approximately 250 barrels were recovered. An estimated 145 barrels was entrained in the soil and an estimated 305 barrels volitalized. It was determined in the field that the mixer assembly had failed causing the release of crude oil from the tank. The mixer assembly was removed and sent for 3rd party failure analysis. Analysis concluded that the cause was the failure of the upper c-clip of the mixer motor assembly, causing excessive vibration and ultimate failure of the mixer hinge. Other mixers of same design and manufacturer in the splp system have been inspected and repaired or retrofitted with manufacturer hinge pin replacement kits.
Report Received Date 2016-09-06 00:00:00
Iyear 2016
Report Number 20160280
Supplemental Number 22427
Report Type Supplemental Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-08-08 06:12:00
Location Latitude 32.529914 Google Maps OpenStreetMap
Location Longitude -100.830396 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 700
Recovered Bbls 395
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2016-08-08 06:12:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Isolated And Pumped Down.
On Site Datetime 2016-08-08 06:25:00
Nrc Rpt Datetime 2016-08-08 08:29:00
Nrc Rpt Num 1155592 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Colorado City Station-Tank 15
Segment Name 23010-26" Colorado City To Wortham
Onshore State Abbreviation Tx
Onshore Postal Code 79526
Onshore City Name Hermleigh
Onshore County Name Scurry
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7900
Est Cost Prop Damage 157000
Est Cost Emergency 50000
Est Cost Environmental 425000
Est Cost Other 0
Prpty 639900
Accident Psig 20
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Controller Did Not Notify Field After Receiving Initial Tank Creep Alarm.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Failure Of Upper Clip On Mixer Hinge Caused It To Laterally Separate Away From The Tank Causing Vibration Which Led To Complete Failure Of The Mixer Hinge Mechanism.
Additional Vibration Ind Yes
Additional Support Ind Yes
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2017-06-19 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On the morning of august 8, 2016 delivery from tank 15 was completed at approximately 02:35. Control center received tank creep alarms and contacted field operations personnel to investigate. At approximately 06:25 field personnel discovered release from tank 15 mixer area. Additional field personnel and resources were dispatched to location while tank 15 was pumped out to below tank mixer level to stop release. All free crude oil was recovered via vacuum truck and contaminated soil was remediated on site. Total volume released was 700 barrels. Approximately 250 barrels were recovered. An estimated 145 barrels was entrained in the soil and an estimated 305 barrels volitalized. It was determined in the field that the mixer assembly had failed causing the release of crude oil from the tank. The mixer assembly was removed and sent for 3rd party failure analysis. Analysis concluded that the cause was the failure of the upper c-clip of the mixer motor assembly, causing excessive vibration and ultimate failure of the mixer hinge. Other mixers of same design and manufacturer in the splp system have been inspected and repaired or retrofitted with manufacturer hinge pin replacement kits.

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