HL incident on 2016-08-09 — TX

Operator
Equistar Chemicals, L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2016-08-09 18:40
Report number
Location
TX
Narrative
At approximately 6:40 p.M. On august 9, 2016, a leak was discovered on a pipeline pig trap closure located at a meter delivery station flowing material to a customer. An in-line inspection tool was run through the pipeline approximately 2.5 hours earlier to meet texas railroad commission pipeline safety regulations. The pipeline pig trap closure o-ring was determined to be the source of the leak and the failure was attributed to high pressure ethylene infiltration into the o-ring material, which resulted in damage to the o-ring when the trap was depressured and opened. The o-ring remained in place throughout three tool runs and the visible portion of the o-ring was inspected each time before the trap was closed. No indication of mechanical damage from repeated closing of the trap was observed.
Detailed record list
Report Received Date
2016-09-01 00:00:00
Iyear
2016
Report Number
20160273
Supplemental Number
21653
Report Type
Original
Operator Id
Name
Equistar Chemicals, L.p.
Operator Street Address
16055 Space Center Blvd. Suite 350
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77062
Local Datetime
2016-08-09 18:40:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
6.15
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
3rd Party, Delivery Site Operations Personnel
Incident Identified Datetime
2016-08-09 18:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-08-09 19:09:00
Restart Datetime
2016-08-09 19:47:00
On Site Datetime
2016-08-09 19:10:00
Nrc Rpt Datetime
2016-08-09 20:05:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Chocolate Bayou System
Segment Name
56_dupont(Kipner) Laporte Lateral Cc Tap
Onshore State Abbreviation
Tx
Onshore Postal Code
77571
Onshore City Name
Laporte
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
1.46
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Installation Year
2011
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
1500
Est Cost Emergency
800
Est Cost Environmental
0
Est Cost Other
0
Prpty
2500
Accident Psig
1564
Mop Psig
2160
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
56
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The location of the leak and all operating conditions were stable at the time of the incident. Additionally, the incident occurred at the beginning of the shift so fatigue was not considered a factor in this incident. The leak was caused by an o-ring failure in pig trap closure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Breakdown Ind
Yes
Preparer Name
G****** L* L******
Preparer Title
Hse Engineer
Preparer Email
G**************@l**.com
Preparer Telephone
281-709-0703
Preparer Fax
281-709-0759
Prepared Date
2016-09-01 00:00:00
Authorizer Name
M****** S* C*****
Authorizer Telephone
281-709-0626
Authorizer Title
Technical And Hse Manager
Authorizer Email
M*************@l**.com
Narrative
At approximately 6:40 p.M. On august 9, 2016, a leak was discovered on a pipeline pig trap closure located at a meter delivery station flowing material to a customer. An in-line inspection tool was run through the pipeline approximately 2.5 hours earlier to meet texas railroad commission pipeline safety regulations. The pipeline pig trap closure o-ring was determined to be the source of the leak and the failure was attributed to high pressure ethylene infiltration into the o-ring material, which resulted in damage to the o-ring when the trap was depressured and opened. The o-ring remained in place throughout three tool runs and the visible portion of the o-ring was inspected each time before the trap was closed. No indication of mechanical damage from repeated closing of the trap was observed.
Report Received Date 2016-09-01 00:00:00
Iyear 2016
Report Number 20160273
Supplemental Number 21653
Report Type Original
Operator Id 25146 PHMSA Enforcement
Name Equistar Chemicals, L.p.
Operator Street Address 16055 Space Center Blvd. Suite 350
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77062
Local Datetime 2016-08-09 18:40:00
Location Latitude 29.70158 Google Maps OpenStreetMap
Location Longitude -95.0414 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 6.15
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details 3rd Party, Delivery Site Operations Personnel
Incident Identified Datetime 2016-08-09 18:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-08-09 19:09:00
Restart Datetime 2016-08-09 19:47:00
On Site Datetime 2016-08-09 19:10:00
Nrc Rpt Datetime 2016-08-09 20:05:00
Nrc Rpt Num 1155777 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Chocolate Bayou System
Segment Name 56_dupont(Kipner) Laporte Lateral Cc Tap
Onshore State Abbreviation Tx
Onshore Postal Code 77571
Onshore City Name Laporte
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 1.46
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Scraper/pig Trap
Installation Year 2011
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 1500
Est Cost Emergency 800
Est Cost Environmental 0
Est Cost Other 0
Prpty 2500
Accident Psig 1564
Mop Psig 2160
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 56
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The location of the leak and all operating conditions were stable at the time of the incident. Additionally, the incident occurred at the beginning of the shift so fatigue was not considered a factor in this incident. The leak was caused by an o-ring failure in pig trap closure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Additional Breakdown Ind Yes
Preparer Name G****** L* L******
Preparer Title Hse Engineer
Preparer Email G**************@l**.com
Preparer Telephone 281-709-0703
Preparer Fax 281-709-0759
Prepared Date 2016-09-01 00:00:00
Authorizer Name M****** S* C*****
Authorizer Telephone 281-709-0626
Authorizer Title Technical And Hse Manager
Authorizer Email M*************@l**.com
Narrative At approximately 6:40 p.M. On august 9, 2016, a leak was discovered on a pipeline pig trap closure located at a meter delivery station flowing material to a customer. An in-line inspection tool was run through the pipeline approximately 2.5 hours earlier to meet texas railroad commission pipeline safety regulations. The pipeline pig trap closure o-ring was determined to be the source of the leak and the failure was attributed to high pressure ethylene infiltration into the o-ring material, which resulted in damage to the o-ring when the trap was depressured and opened. The o-ring remained in place throughout three tool runs and the visible portion of the o-ring was inspected each time before the trap was closed. No indication of mechanical damage from repeated closing of the trap was observed.

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