HL incident on 2016-08-05 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2016-08-05 17:45
Report number
Location
TX
Narrative
During routine operations at corsicana station on 8/5/2016, operating personnel discovered a fine spray of crude oil at tank 2733 header platform from a thermal relief valve. The valve was isolated, removed and a new stainless steel differential check valve and associated stainless steel tubing was installed. The minimal amount of oil was removed via absorbent pads and the contaminated soil was removed for onsite remediation. An inspection was performed of the facility to identify similar or identical valves. Via this investigation a similar valve was identified and replaced on the adjacent tank line. A full check of the associated incoming pipeline system will be conducted for similar or identical thermal relief valve installations. If identified these valves will be removed and replaced.
Detailed record list
Report Received Date
2016-08-31 00:00:00
Iyear
2016
Report Number
20160269
Supplemental Number
21646
Report Type
Original Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-08-05 17:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-08-05 17:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank 2733 Suction Line Was Isolated
On Site Datetime
2016-08-05 17:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Corsicana Tank Farm
Segment Name
26" Tank 2733 Suction Line
Onshore State Abbreviation
Tx
Onshore Postal Code
75110
Onshore City Name
Corsicana
Onshore County Name
Navarro
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
14
Est Cost Prop Damage
500
Est Cost Emergency
100
Est Cost Environmental
500
Est Cost Other
0
Prpty
1114
Accident Psig
25
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Equipment Beyond Serviceable Life
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-08-31 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
During routine operations at corsicana station on 8/5/2016, operating personnel discovered a fine spray of crude oil at tank 2733 header platform from a thermal relief valve. The valve was isolated, removed and a new stainless steel differential check valve and associated stainless steel tubing was installed. The minimal amount of oil was removed via absorbent pads and the contaminated soil was removed for onsite remediation. An inspection was performed of the facility to identify similar or identical valves. Via this investigation a similar valve was identified and replaced on the adjacent tank line. A full check of the associated incoming pipeline system will be conducted for similar or identical thermal relief valve installations. If identified these valves will be removed and replaced.
Report Received Date 2016-08-31 00:00:00
Iyear 2016
Report Number 20160269
Supplemental Number 21646
Report Type Original Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-08-05 17:45:00
Location Latitude 32.06854 Google Maps OpenStreetMap
Location Longitude -96.47929 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-08-05 17:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank 2733 Suction Line Was Isolated
On Site Datetime 2016-08-05 17:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Corsicana Tank Farm
Segment Name 26" Tank 2733 Suction Line
Onshore State Abbreviation Tx
Onshore Postal Code 75110
Onshore City Name Corsicana
Onshore County Name Navarro
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 14
Est Cost Prop Damage 500
Est Cost Emergency 100
Est Cost Environmental 500
Est Cost Other 0
Prpty 1114
Accident Psig 25
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Equipment Beyond Serviceable Life
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-08-31 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative During routine operations at corsicana station on 8/5/2016, operating personnel discovered a fine spray of crude oil at tank 2733 header platform from a thermal relief valve. The valve was isolated, removed and a new stainless steel differential check valve and associated stainless steel tubing was installed. The minimal amount of oil was removed via absorbent pads and the contaminated soil was removed for onsite remediation. An inspection was performed of the facility to identify similar or identical valves. Via this investigation a similar valve was identified and replaced on the adjacent tank line. A full check of the associated incoming pipeline system will be conducted for similar or identical thermal relief valve installations. If identified these valves will be removed and replaced.

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