HL incident on 2016-08-02 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2016-08-02 03:30
Report number
Location
TX
Narrative
On 08/02/2016 at approximately 03:30 local operating personnel noticed crude oil had released from an open 2" drain valve. After investigation it was determined that operations unintentionally left the drain valve open after preparing for maintenance work and residual crude from the drained pipe was spilled. The valve was closed and leak was stopped. All crude was remediated and the facility returned back to normal.
Detailed record list
Report Received Date
2016-08-29 00:00:00
Iyear
2016
Report Number
20160267
Supplemental Number
21643
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-08-02 03:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-08-02 03:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Closed To Isolate The Leak
On Site Datetime
2016-08-02 03:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Appelt
Segment Name
390-104 Manifold Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Appelt
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2013
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Valve Left Open
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
180
Est Cost Prop Damage
40000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
40180
Accident Psig
5
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller nor control room were a contributing factor
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type
Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related No Proc Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
C**** A******
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2016-08-29 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
C*******@e****.com
Narrative
On 08/02/2016 at approximately 03:30 local operating personnel noticed crude oil had released from an open 2" drain valve. After investigation it was determined that operations unintentionally left the drain valve open after preparing for maintenance work and residual crude from the drained pipe was spilled. The valve was closed and leak was stopped. All crude was remediated and the facility returned back to normal.
Report Received Date 2016-08-29 00:00:00
Iyear 2016
Report Number 20160267
Supplemental Number 21643
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-08-02 03:30:00
Location Latitude 29.758902 Google Maps OpenStreetMap
Location Longitude -95.143291 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-08-02 03:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Closed To Isolate The Leak
On Site Datetime 2016-08-02 03:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Appelt
Segment Name 390-104 Manifold Piping
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Appelt
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2013
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Valve Left Open
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 180
Est Cost Prop Damage 40000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 40180
Accident Psig 5
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller nor control room were a contributing factor
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Operation Type Valve Left Or Placed In Wrong Position, But Not Resulting In A Tank, Vessel, Or Sump/separator Overflow Or Facility Overpressure
Related No Proc Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name C**** A******
Preparer Email C*******@e****.com
Preparer Telephone 713-381-6426
Prepared Date 2016-08-29 00:00:00
Authorizer Name C**** A******
Authorizer Telephone 713-381-6426
Authorizer Title Pipeline Compliance Specialist
Authorizer Email C*******@e****.com
Narrative On 08/02/2016 at approximately 03:30 local operating personnel noticed crude oil had released from an open 2" drain valve. After investigation it was determined that operations unintentionally left the drain valve open after preparing for maintenance work and residual crude from the drained pipe was spilled. The valve was closed and leak was stopped. All crude was remediated and the facility returned back to normal.

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