HL incident on 2016-07-26 — TX

Operator
Sunoco Pipeline L.p.
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-07-26 13:45
Report number
Location
TX
Narrative
Local operating personnel were performing a station check and discovered a release from a small diameter bleeder valve on the incoming meter setting. Investigation revealed that a closed needle valve had loosened or otherwise failed releasing approximately 5 gallons of crude oil. The needle valve was removed and replaced. A rated quick connect fitting and plug were also installed downstream of the needle valve to ensure two sources of isolation when checking the block and bleed valve operation and/or sampling. The contaminated soil was removed for onsite remediation.
Detailed record list
Report Received Date
2016-08-24 00:00:00
Iyear
2016
Report Number
20160263
Supplemental Number
21636
Report Type
Original Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-07-26 13:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-07-26 13:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Location Of Failure Was Isolated From Mainline Operation.
On Site Datetime
2016-07-26 13:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Holly-West Tulsa
Segment Name
24019 12" Drumright To Tulsa
Onshore State Abbreviation
Ok
Onshore Postal Code
74107
Onshore City Name
Tulsa
Onshore County Name
Tulsa
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Bleeder Valve Loosened
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
0
Accident Psig
70
Mop Psig
150
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Unknown
Other Type
Unknown
Unknown Subtype
Investigation Complete, Cause Of Accident Unknown
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-08-24 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
Local operating personnel were performing a station check and discovered a release from a small diameter bleeder valve on the incoming meter setting. Investigation revealed that a closed needle valve had loosened or otherwise failed releasing approximately 5 gallons of crude oil. The needle valve was removed and replaced. A rated quick connect fitting and plug were also installed downstream of the needle valve to ensure two sources of isolation when checking the block and bleed valve operation and/or sampling. The contaminated soil was removed for onsite remediation.
Report Received Date 2016-08-24 00:00:00
Iyear 2016
Report Number 20160263
Supplemental Number 21636
Report Type Original Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-07-26 13:45:00
Location Latitude 36.13824 Google Maps OpenStreetMap
Location Longitude -96.02963 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-07-26 13:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Location Of Failure Was Isolated From Mainline Operation.
On Site Datetime 2016-07-26 13:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Holly-West Tulsa
Segment Name 24019 12" Drumright To Tulsa
Onshore State Abbreviation Ok
Onshore Postal Code 74107
Onshore City Name Tulsa
Onshore County Name Tulsa
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Other
Leak Type Other Bleeder Valve Loosened
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 0
Accident Psig 70
Mop Psig 150
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Unknown
Other Type Unknown
Unknown Subtype Investigation Complete, Cause Of Accident Unknown
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-08-24 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative Local operating personnel were performing a station check and discovered a release from a small diameter bleeder valve on the incoming meter setting. Investigation revealed that a closed needle valve had loosened or otherwise failed releasing approximately 5 gallons of crude oil. The needle valve was removed and replaced. A rated quick connect fitting and plug were also installed downstream of the needle valve to ensure two sources of isolation when checking the block and bleed valve operation and/or sampling. The contaminated soil was removed for onsite remediation.

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