HL incident on 2016-07-25 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2016-07-25 12:01
Report number
Location
TX
Narrative
Operator personnel discovered product pooling in the concrete pig barrel containment at approximately 12:01 am. At the time, it was believed approximately 1 gallon of product was released. Following further investigation, it was determined at 6:45 am that approximately 2 bbls of product had been released into the containment pad and onto the surrounding gravel. A newly-installed thermal relief valve on the p91 pig barrel had leaked-by, allowing product into a shared drain system. The drain system was blocked by blasting media from a recent painting project and backed up into the pig barrel containment. The relief was isolated and repaired, product cleaned up, and the drain line cleared and verified open.
Detailed record list
Report Received Date
2016-08-16 00:00:00
Iyear
2016
Report Number
20160255
Supplemental Number
21602
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-07-25 12:01:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-07-25 12:01:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Did Not Affect Pipeline Operations.
On Site Datetime
2016-07-25 12:01:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Baytown Terminal
Segment Name
P91 Pig Barrel Thermal Relief
Onshore State Abbreviation
Tx
Onshore Postal Code
77520
Onshore City Name
Baytown
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Baytown Term
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Relief Line And Relief Equipment
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
New Relief Valve Did Not Seal
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
94
Est Cost Prop Damage
500
Est Cost Emergency
0
Est Cost Environmental
200
Est Cost Other
0
Prpty
794
Accident Psig
42
Mop Psig
1125
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Release Occurred On Relief Line.
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
Release Occurred On Relief Line
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller actions did not contribute to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Additional Defect Ind
Yes
Preparer Name
M*** P*****
Preparer Title
Sr. Compliance Specialist
Preparer Email
M*******@e****.com
Preparer Telephone
713-381-5897
Prepared Date
2016-08-16 00:00:00
Authorizer Name
M*** P*****
Authorizer Telephone
713-381-5897
Authorizer Title
Sr. Compliance Specialist
Authorizer Email
M*******@e****.com
Narrative
Operator personnel discovered product pooling in the concrete pig barrel containment at approximately 12:01 am. At the time, it was believed approximately 1 gallon of product was released. Following further investigation, it was determined at 6:45 am that approximately 2 bbls of product had been released into the containment pad and onto the surrounding gravel. A newly-installed thermal relief valve on the p91 pig barrel had leaked-by, allowing product into a shared drain system. The drain system was blocked by blasting media from a recent painting project and backed up into the pig barrel containment. The relief was isolated and repaired, product cleaned up, and the drain line cleared and verified open.
Report Received Date 2016-08-16 00:00:00
Iyear 2016
Report Number 20160255
Supplemental Number 21602
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-07-25 12:01:00
Location Latitude 29.766845 Google Maps OpenStreetMap
Location Longitude -95.012746 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-07-25 12:01:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Did Not Affect Pipeline Operations.
On Site Datetime 2016-07-25 12:01:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Baytown Terminal
Segment Name P91 Pig Barrel Thermal Relief
Onshore State Abbreviation Tx
Onshore Postal Code 77520
Onshore City Name Baytown
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Baytown Term
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Relief Line And Relief Equipment
Installation Year 2016
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other New Relief Valve Did Not Seal
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 94
Est Cost Prop Damage 500
Est Cost Emergency 0
Est Cost Environmental 200
Est Cost Other 0
Prpty 794
Accident Psig 42
Mop Psig 1125
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Release Occurred On Relief Line.
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details Release Occurred On Relief Line
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller actions did not contribute to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Additional Defect Ind Yes
Preparer Name M*** P*****
Preparer Title Sr. Compliance Specialist
Preparer Email M*******@e****.com
Preparer Telephone 713-381-5897
Prepared Date 2016-08-16 00:00:00
Authorizer Name M*** P*****
Authorizer Telephone 713-381-5897
Authorizer Title Sr. Compliance Specialist
Authorizer Email M*******@e****.com
Narrative Operator personnel discovered product pooling in the concrete pig barrel containment at approximately 12:01 am. At the time, it was believed approximately 1 gallon of product was released. Following further investigation, it was determined at 6:45 am that approximately 2 bbls of product had been released into the containment pad and onto the surrounding gravel. A newly-installed thermal relief valve on the p91 pig barrel had leaked-by, allowing product into a shared drain system. The drain system was blocked by blasting media from a recent painting project and backed up into the pig barrel containment. The relief was isolated and repaired, product cleaned up, and the drain line cleared and verified open.

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