HL incident on 2016-07-17 — TX

Operator
Exxonmobil Pipeline Co
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2016-07-17 09:30
Report number
Location
TX
Narrative
Empco was notified of a refinery grade propylene (rgp) release at above ground piping near bayway dr. In baytown. Empco began shutting down rgp flow by closing block valves. The baytown fire dept. Issued a limited shelter-in-place and evacuation orders which were both lifted after confirming that the release had stopped at approximately 1500. The release was caused by a failed pressure warning device (pwd) gasket on a tube turn hinged closure installed on the scraper trap.
Detailed record list
Report Received Date
2016-08-16 00:00:00
Iyear
2016
Report Number
20160254
Supplemental Number
21852
Report Type
Supplemental Final
Operator Id
Name
Exxonmobil Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2016-07-17 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Dilute Propylene
Unintentional Release Bbls
90
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2016-07-17 09:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-07-17 09:45:00
Restart Datetime
2016-07-17 19:30:00
On Site Datetime
2016-07-17 10:15:00
Nrc Rpt Datetime
2016-07-17 11:25:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
30
Pipe Fac Name
Tx-135a Mt Belvieu To Clearlake
Segment Name
Bayway Trap
Onshore State Abbreviation
Tx
Onshore Postal Code
77520
Onshore City Name
Baytown
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Bayway Trap
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Installation Year
1980
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket Material
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
3500
Est Cost Prop Damage
100
Est Cost Emergency
3400
Est Cost Environmental
0
Est Cost Other
0
Prpty
7000
Accident Psig
874
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
41659
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the scada data did not show any unusual alarms or events that should have alerted the controller.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
The Release Was Caused By The Failure Of A Gasket In A Pressure Warning Device On The Scraper Trap Door.
Additional Breakdown Ind
Yes
Preparer Name
T*** M*********
Preparer Title
Pipeline Safety Advisor
Preparer Email
T**************@e*********.com
Preparer Telephone
8326247880
Preparer Fax
8326486336
Prepared Date
2016-11-15 00:00:00
Authorizer Name
M*** D* W******
Authorizer Telephone
8326247868
Authorizer Title
Sshe Manager
Authorizer Email
M*************@e*********.com
Narrative
Empco was notified of a refinery grade propylene (rgp) release at above ground piping near bayway dr. In baytown. Empco began shutting down rgp flow by closing block valves. The baytown fire dept. Issued a limited shelter-in-place and evacuation orders which were both lifted after confirming that the release had stopped at approximately 1500. The release was caused by a failed pressure warning device (pwd) gasket on a tube turn hinged closure installed on the scraper trap.
Report Received Date 2016-08-16 00:00:00
Iyear 2016
Report Number 20160254
Supplemental Number 21852
Report Type Supplemental Final
Operator Id 4906 PHMSA Enforcement
Name Exxonmobil Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E2.2b-Emp
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2016-07-17 09:30:00
Location Latitude 29.74787 Google Maps OpenStreetMap
Location Longitude -95.0312 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Dilute Propylene
Unintentional Release Bbls 90
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2016-07-17 09:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-07-17 09:45:00
Restart Datetime 2016-07-17 19:30:00
On Site Datetime 2016-07-17 10:15:00
Nrc Rpt Datetime 2016-07-17 11:25:00
Nrc Rpt Num 1153628 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 30
Pipe Fac Name Tx-135a Mt Belvieu To Clearlake
Segment Name Bayway Trap
Onshore State Abbreviation Tx
Onshore Postal Code 77520
Onshore City Name Baytown
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Bayway Trap
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Scraper/pig Trap
Installation Year 1980
Material Involved Material Other Than Carbon Steel
Material Details Gasket Material
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 3500
Est Cost Prop Damage 100
Est Cost Emergency 3400
Est Cost Environmental 0
Est Cost Other 0
Prpty 7000
Accident Psig 874
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 41659
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the scada data did not show any unusual alarms or events that should have alerted the controller.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details The Release Was Caused By The Failure Of A Gasket In A Pressure Warning Device On The Scraper Trap Door.
Additional Breakdown Ind Yes
Preparer Name T*** M*********
Preparer Title Pipeline Safety Advisor
Preparer Email T**************@e*********.com
Preparer Telephone 8326247880
Preparer Fax 8326486336
Prepared Date 2016-11-15 00:00:00
Authorizer Name M*** D* W******
Authorizer Telephone 8326247868
Authorizer Title Sshe Manager
Authorizer Email M*************@e*********.com
Narrative Empco was notified of a refinery grade propylene (rgp) release at above ground piping near bayway dr. In baytown. Empco began shutting down rgp flow by closing block valves. The baytown fire dept. Issued a limited shelter-in-place and evacuation orders which were both lifted after confirming that the release had stopped at approximately 1500. The release was caused by a failed pressure warning device (pwd) gasket on a tube turn hinged closure installed on the scraper trap.

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