HL incident on 2016-07-12 — TX

Operator
Delek Crude Logistics, Llc.
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-07-12 12:30
Report number
Location
TX
Narrative
At approximately 12:30 hours diesel fuel began leaking from the above-ground pipeline receipt header at delek's greenville pump station while reversing the position of a figure 8 skillet blind. The diesel had leaked past a third party valve that was being used to isolate the system. The delek logistics (dkl) greenville pump station is located at 2867 cr 2168, caddo mills, hunt county, tx. An estimated 555 gallons (13.21 bbls) of diesel fuel leaked from the above-ground pipeline header onto the pump station property. No adjoining properties or surface waters were impacted by the discharge. Absorbent booms and pads were immediately deployed, and free liquids were removed via vacuum (vac) truck. Tas, a third-party oil spill response organization (osro), was contracted to perform response actions which consisted of: 1) delineating and removing contamination from the affected area; 2) performing field verification that contamination removal was achieved; 3) backfill and return affected area to pre-response contours. The osro response activities commenced on july 13, 2016 at approximately 09:00 hours and were completed on july 28, 2016.
Detailed record list
Report Received Date
2016-08-11 00:00:00
Iyear
2016
Report Number
20160247
Supplemental Number
33129
Report Type
Supplemental Final
Operator Id
Name
Delek Crude Logistics, Llc.
Operator Street Address
5850 Granite Parkway #450
Operator City Name
Plano
Operator State Abbreviation
TX
Operator Postal Code
75024
Local Datetime
2016-07-12 12:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
13.21
Recovered Bbls
13.21
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-07-12 12:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Has Been Down And Has Been For Several Months.
On Site Datetime
2016-07-12 12:30:00
Nrc Rpt Datetime
2016-07-13 12:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Greenville Station
Segment Name
Greenville Station
Onshore State Abbreviation
Tx
Onshore Postal Code
75135
Onshore City Name
Caddo Mills
Onshore County Name
Hunt
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1981
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Maintenance Activity That Resulted In A Leak. Maintenance Crews Were Switching A Figure 8 Skillet Blind And The Pipeline Started Leaking Once The Flange Bolts Where Loose Because Explorer's Connection Valve Was Leaking Cause To Be Determined By Explorer.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
694
Est Cost Prop Damage
0
Est Cost Emergency
79000
Est Cost Environmental
15840
Est Cost Other
0
Prpty
95534
Accident Psig
1
Mop Psig
280
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No because the pipeline system was down and has been for several months and it happened due to normal maintenance activity and a faulty valve from the 3rd party's connection valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Inadequate Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
M****** S******
Preparer Title
Director Regulatory Compliance And Row Management
Preparer Email
M**************@d*************.com
Preparer Telephone
6306498016
Prepared Date
2019-12-24 00:00:00
Authorizer Name
M****** S******
Authorizer Telephone
6306498016
Authorizer Title
Director Regulatory Compliance And Row Management
Authorizer Email
M**************@d*************.com
Narrative
At approximately 12:30 hours diesel fuel began leaking from the above-ground pipeline receipt header at delek's greenville pump station while reversing the position of a figure 8 skillet blind. The diesel had leaked past a third party valve that was being used to isolate the system. The delek logistics (dkl) greenville pump station is located at 2867 cr 2168, caddo mills, hunt county, tx. An estimated 555 gallons (13.21 bbls) of diesel fuel leaked from the above-ground pipeline header onto the pump station property. No adjoining properties or surface waters were impacted by the discharge. Absorbent booms and pads were immediately deployed, and free liquids were removed via vacuum (vac) truck. Tas, a third-party oil spill response organization (osro), was contracted to perform response actions which consisted of: 1) delineating and removing contamination from the affected area; 2) performing field verification that contamination removal was achieved; 3) backfill and return affected area to pre-response contours. The osro response activities commenced on july 13, 2016 at approximately 09:00 hours and were completed on july 28, 2016.
Report Received Date 2016-08-11 00:00:00
Iyear 2016
Report Number 20160247
Supplemental Number 33129
Report Type Supplemental Final
Operator Id 26061 PHMSA Enforcement
Name Delek Crude Logistics, Llc.
Operator Street Address 5850 Granite Parkway #450
Operator City Name Plano
Operator State Abbreviation TX
Operator Postal Code 75024
Local Datetime 2016-07-12 12:30:00
Location Latitude 33.034328 Google Maps OpenStreetMap
Location Longitude -96.202772 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 13.21
Recovered Bbls 13.21
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-07-12 12:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Has Been Down And Has Been For Several Months.
On Site Datetime 2016-07-12 12:30:00
Nrc Rpt Datetime 2016-07-13 12:15:00
Nrc Rpt Num 1153196 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Greenville Station
Segment Name Greenville Station
Onshore State Abbreviation Tx
Onshore Postal Code 75135
Onshore City Name Caddo Mills
Onshore County Name Hunt
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1981
Material Involved Carbon Steel
Release Type Other
Release Type Details Maintenance Activity That Resulted In A Leak. Maintenance Crews Were Switching A Figure 8 Skillet Blind And The Pipeline Started Leaking Once The Flange Bolts Where Loose Because Explorer's Connection Valve Was Leaking Cause To Be Determined By Explorer.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 694
Est Cost Prop Damage 0
Est Cost Emergency 79000
Est Cost Environmental 15840
Est Cost Other 0
Prpty 95534
Accident Psig 1
Mop Psig 280
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No because the pipeline system was down and has been for several months and it happened due to normal maintenance activity and a faulty valve from the 3rd party's connection valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Inadequate Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name M****** S******
Preparer Title Director Regulatory Compliance And Row Management
Preparer Email M**************@d*************.com
Preparer Telephone 6306498016
Prepared Date 2019-12-24 00:00:00
Authorizer Name M****** S******
Authorizer Telephone 6306498016
Authorizer Title Director Regulatory Compliance And Row Management
Authorizer Email M**************@d*************.com
Narrative At approximately 12:30 hours diesel fuel began leaking from the above-ground pipeline receipt header at delek's greenville pump station while reversing the position of a figure 8 skillet blind. The diesel had leaked past a third party valve that was being used to isolate the system. The delek logistics (dkl) greenville pump station is located at 2867 cr 2168, caddo mills, hunt county, tx. An estimated 555 gallons (13.21 bbls) of diesel fuel leaked from the above-ground pipeline header onto the pump station property. No adjoining properties or surface waters were impacted by the discharge. Absorbent booms and pads were immediately deployed, and free liquids were removed via vacuum (vac) truck. Tas, a third-party oil spill response organization (osro), was contracted to perform response actions which consisted of: 1) delineating and removing contamination from the affected area; 2) performing field verification that contamination removal was achieved; 3) backfill and return affected area to pre-response contours. The osro response activities commenced on july 13, 2016 at approximately 09:00 hours and were completed on july 28, 2016.

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