HL incident on 2016-07-14 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2016-07-14 08:10
Report number
Location
OK
Narrative
The release occurred at approximately 8:10 mst while the tank was receiving product during commissioning. When the level in tank 2503 reached a point on the tank nozzle of 3 ft. Product began to run out through a 1" open threaded weld-o-let located on the 18"x16" tank nozzle. Contractor personnel on site notified local operations and product movement into the tank was shut down. A one inch valve and plug were installed on the weld-o-let after the release was identified. The weld-o-let was plugged during the successful hydro-testing of the tank. During the p&id and pre-startup safety review walk through, a valve was identified as being in place in the weld-o-let. However, at some subsequent point the valve was removed by persons unknown and the weld-o-let left open during the filling of the tank with product. A visual inspection was done prior to receiving product into tankage but the missing valve was not detected at that time. Most of the released product collected on visqueen spread around the perimeter of the tank and was recovered by a vacuum truck. The product that impacted the soil was excavated and put into a roll-off container. Approximately 5 yards of soil was remediated.
Detailed record list
Report Received Date
2016-08-09 00:00:00
Iyear
2016
Report Number
20160246
Supplemental Number
21582
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2016-07-14 08:10:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.19
Recovered Bbls
1.19
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2016-07-14 08:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-07-14 08:20:00
Restart Datetime
2016-07-14 10:30:00
On Site Datetime
2016-07-14 08:10:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Platteville Terminal
Segment Name
Station No. 880
Onshore State Abbreviation
Co
Onshore Postal Code
80642
Onshore City Name
Hudson
Onshore County Name
Weld
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Appurtenance
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Weld-O-Let Was Left Open.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
21
Est Cost Prop Damage
100
Est Cost Emergency
5072
Est Cost Environmental
0
Est Cost Other
0
Prpty
5193
Accident Psig
1
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was below system detection limits.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Other Ind
Yes
Operation Related Details
Failed To Adequately Inspect Tank Before Receipt.
Category Type
Commissioning
Operator Qualification Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2016-08-09 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
The release occurred at approximately 8:10 mst while the tank was receiving product during commissioning. When the level in tank 2503 reached a point on the tank nozzle of 3 ft. Product began to run out through a 1" open threaded weld-o-let located on the 18"x16" tank nozzle. Contractor personnel on site notified local operations and product movement into the tank was shut down. A one inch valve and plug were installed on the weld-o-let after the release was identified. The weld-o-let was plugged during the successful hydro-testing of the tank. During the p&id and pre-startup safety review walk through, a valve was identified as being in place in the weld-o-let. However, at some subsequent point the valve was removed by persons unknown and the weld-o-let left open during the filling of the tank with product. A visual inspection was done prior to receiving product into tankage but the missing valve was not detected at that time. Most of the released product collected on visqueen spread around the perimeter of the tank and was recovered by a vacuum truck. The product that impacted the soil was excavated and put into a roll-off container. Approximately 5 yards of soil was remediated.
Report Received Date 2016-08-09 00:00:00
Iyear 2016
Report Number 20160246
Supplemental Number 21582
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2016-07-14 08:10:00
Location Latitude 40.20069 Google Maps OpenStreetMap
Location Longitude -104.60941 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.19
Recovered Bbls 1.19
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2016-07-14 08:10:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-07-14 08:20:00
Restart Datetime 2016-07-14 10:30:00
On Site Datetime 2016-07-14 08:10:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Platteville Terminal
Segment Name Station No. 880
Onshore State Abbreviation Co
Onshore Postal Code 80642
Onshore City Name Hudson
Onshore County Name Weld
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Appurtenance
Installation Year 2016
Material Involved Carbon Steel
Release Type Other
Release Type Details Weld-O-Let Was Left Open.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 21
Est Cost Prop Damage 100
Est Cost Emergency 5072
Est Cost Environmental 0
Est Cost Other 0
Prpty 5193
Accident Psig 1
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was below system detection limits.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Other Ind Yes
Operation Related Details Failed To Adequately Inspect Tank Before Receipt.
Category Type Commissioning
Operator Qualification Ind No
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2016-08-09 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative The release occurred at approximately 8:10 mst while the tank was receiving product during commissioning. When the level in tank 2503 reached a point on the tank nozzle of 3 ft. Product began to run out through a 1" open threaded weld-o-let located on the 18"x16" tank nozzle. Contractor personnel on site notified local operations and product movement into the tank was shut down. A one inch valve and plug were installed on the weld-o-let after the release was identified. The weld-o-let was plugged during the successful hydro-testing of the tank. During the p&id and pre-startup safety review walk through, a valve was identified as being in place in the weld-o-let. However, at some subsequent point the valve was removed by persons unknown and the weld-o-let left open during the filling of the tank with product. A visual inspection was done prior to receiving product into tankage but the missing valve was not detected at that time. Most of the released product collected on visqueen spread around the perimeter of the tank and was recovered by a vacuum truck. The product that impacted the soil was excavated and put into a roll-off container. Approximately 5 yards of soil was remediated.

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