HL incident on 2016-06-20 — TX

Operator
Tesoro High Plains Pipeline Company Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-06-20 10:00
Report number
Location
TX
Narrative
On june 20th, 2016 a crude oil spill was discovered on the ground at dunn center station. The mechanical seal on booster pump #2 leaked to ground. There were no impacts to surface or ground water. It was fully contained on tesoro property. It was cleaned up immediately upon discovery. Update: on friday, june 17th the pump was taken out of service for maintenance. After approximately 3 hours, it was determined that the work would resume on monday. At that time no leaking from the seal had occurred. The pump was left locked out and tagged out(loto) from the motor over the weekend. The extended loto allowed the mechanical seal, which requires tension to function properly, to leak.
Detailed record list
Report Received Date
2016-07-20 00:00:00
Iyear
2016
Report Number
20160231
Supplemental Number
21776
Report Type
Supplemental Final
Operator Id
Name
Tesoro High Plains Pipeline Company Llc
Operator Street Address
19100 Ridgewood Parkway
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78259
Local Datetime
2016-06-20 10:00:00
Location Latitude
Location Longitude
-102.5044111
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-06-20 10:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pump Was Already Shutdown And Lock Out & Tagged Out.
On Site Datetime
2016-06-20 10:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Tesoro High Plains Pipeline
Segment Name
Dunn Center
Onshore State Abbreviation
Nd
Onshore Postal Code
58636
Onshore City Name
Not Within A Municipality
Onshore County Name
Dunn
Designated Location
Milepost/valve Station
Designated Name
Dunn Center
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
1981
Material Involved
Material Other Than Carbon Steel
Material Details
Pump Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
5
Est Cost Prop Damage
0
Est Cost Emergency
250
Est Cost Environmental
170
Est Cost Other
0
Prpty
425
Accident Psig
10
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
No Tension On The Mechanical Seal While In Loto
Preparer Name
A***** R********
Preparer Title
Sr. Regulatory Compliance Specialist
Preparer Email
A***************@t******.com
Preparer Telephone
210-626-4262
Prepared Date
2016-10-20 00:00:00
Authorizer Name
A**** M*******
Authorizer Telephone
210-626-6343
Authorizer Title
Director Compliance Logistics
Authorizer Email
A***************@t******.com
Narrative
On june 20th, 2016 a crude oil spill was discovered on the ground at dunn center station. The mechanical seal on booster pump #2 leaked to ground. There were no impacts to surface or ground water. It was fully contained on tesoro property. It was cleaned up immediately upon discovery. Update: on friday, june 17th the pump was taken out of service for maintenance. After approximately 3 hours, it was determined that the work would resume on monday. At that time no leaking from the seal had occurred. The pump was left locked out and tagged out(loto) from the motor over the weekend. The extended loto allowed the mechanical seal, which requires tension to function properly, to leak.
Report Received Date 2016-07-20 00:00:00
Iyear 2016
Report Number 20160231
Supplemental Number 21776
Report Type Supplemental Final
Operator Id 31570 PHMSA Enforcement
Name Tesoro High Plains Pipeline Company Llc
Operator Street Address 19100 Ridgewood Parkway
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78259
Local Datetime 2016-06-20 10:00:00
Location Latitude 47.4593167 Google Maps OpenStreetMap
Location Longitude -102.5044111 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-06-20 10:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pump Was Already Shutdown And Lock Out & Tagged Out.
On Site Datetime 2016-06-20 10:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Tesoro High Plains Pipeline
Segment Name Dunn Center
Onshore State Abbreviation Nd
Onshore Postal Code 58636
Onshore City Name Not Within A Municipality
Onshore County Name Dunn
Designated Location Milepost/valve Station
Designated Name Dunn Center
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 1981
Material Involved Material Other Than Carbon Steel
Material Details Pump Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 5
Est Cost Prop Damage 0
Est Cost Emergency 250
Est Cost Environmental 170
Est Cost Other 0
Prpty 425
Accident Psig 10
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details No Tension On The Mechanical Seal While In Loto
Preparer Name A***** R********
Preparer Title Sr. Regulatory Compliance Specialist
Preparer Email A***************@t******.com
Preparer Telephone 210-626-4262
Prepared Date 2016-10-20 00:00:00
Authorizer Name A**** M*******
Authorizer Telephone 210-626-6343
Authorizer Title Director Compliance Logistics
Authorizer Email A***************@t******.com
Narrative On june 20th, 2016 a crude oil spill was discovered on the ground at dunn center station. The mechanical seal on booster pump #2 leaked to ground. There were no impacts to surface or ground water. It was fully contained on tesoro property. It was cleaned up immediately upon discovery. Update: on friday, june 17th the pump was taken out of service for maintenance. After approximately 3 hours, it was determined that the work would resume on monday. At that time no leaking from the seal had occurred. The pump was left locked out and tagged out(loto) from the motor over the weekend. The extended loto allowed the mechanical seal, which requires tension to function properly, to leak.

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