HL incident on 2016-06-06 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,761
Incident datetime
2016-06-06 07:00
Report number
Location
TX
Narrative
On 06/06/2016 company personnel arrived at blum station at approximately 07:00 and discovered crude oil in the containment area. The control center was immediately notified and the mainline was sht down. Emergency response personnel were activated and dispatched to the site. Approximately 200 barrels were released to the containment area and facility retention pond. Investigation revealed a pinhole in a 4" drain line from the bottom of the strainer basket to the sump. The affected piping was removed and associated piping/appurtenances were blinded. The failed pipe was sent for metallurgical analysis and it was determined that the cause was microbial induced, internal corrosion. New strainer piping installed will have an internal liner to prevent recurrence of internal corrosion and future releases.
Detailed record list
Report Received Date
2016-07-06 00:00:00
Iyear
2016
Report Number
20160212
Supplemental Number
21899
Report Type
Supplemental Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-06-06 07:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
200
Recovered Bbls
195
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-06-06 07:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-06-06 07:00:00
Restart Datetime
2016-06-06 22:00:00
On Site Datetime
2016-06-06 07:00:00
Nrc Rpt Datetime
2016-06-06 09:16:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Blum Station
Segment Name
23010-26" Colorado City To Wortham
Onshore State Abbreviation
Tx
Onshore Postal Code
76627
Onshore City Name
Blum
Onshore County Name
Hill
Designated Location
Milepost/valve Station
Designated Name
Mp 202
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4
Pipe Wall Thickness
0.237
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Installation Year
2011
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
200
Rel Water Name
Facility Containment/retention Pond
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
2000
Est Cost Gas Released
231
Est Cost Prop Damage
26761
Est Cost Emergency
83283
Est Cost Environmental
75000
Est Cost Other
0
Prpty
187275
Accident Psig
253
Mop Psig
750
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-11-30 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 06/06/2016 company personnel arrived at blum station at approximately 07:00 and discovered crude oil in the containment area. The control center was immediately notified and the mainline was sht down. Emergency response personnel were activated and dispatched to the site. Approximately 200 barrels were released to the containment area and facility retention pond. Investigation revealed a pinhole in a 4" drain line from the bottom of the strainer basket to the sump. The affected piping was removed and associated piping/appurtenances were blinded. The failed pipe was sent for metallurgical analysis and it was determined that the cause was microbial induced, internal corrosion. New strainer piping installed will have an internal liner to prevent recurrence of internal corrosion and future releases.
Report Received Date 2016-07-06 00:00:00
Iyear 2016
Report Number 20160212
Supplemental Number 21899
Report Type Supplemental Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-06-06 07:00:00
Location Latitude 32.15284 Google Maps OpenStreetMap
Location Longitude -97.37462 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 200
Recovered Bbls 195
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-06-06 07:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-06-06 07:00:00
Restart Datetime 2016-06-06 22:00:00
On Site Datetime 2016-06-06 07:00:00
Nrc Rpt Datetime 2016-06-06 09:16:00
Nrc Rpt Num 1149839 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Blum Station
Segment Name 23010-26" Colorado City To Wortham
Onshore State Abbreviation Tx
Onshore Postal Code 76627
Onshore City Name Blum
Onshore County Name Hill
Designated Location Milepost/valve Station
Designated Name Mp 202
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4
Pipe Wall Thickness 0.237
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Installation Year 2011
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 200
Rel Water Name Facility Containment/retention Pond
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 2000
Est Cost Gas Released 231
Est Cost Prop Damage 26761
Est Cost Emergency 83283
Est Cost Environmental 75000
Est Cost Other 0
Prpty 187275
Accident Psig 253
Mop Psig 750
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-11-30 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 06/06/2016 company personnel arrived at blum station at approximately 07:00 and discovered crude oil in the containment area. The control center was immediately notified and the mainline was sht down. Emergency response personnel were activated and dispatched to the site. Approximately 200 barrels were released to the containment area and facility retention pond. Investigation revealed a pinhole in a 4" drain line from the bottom of the strainer basket to the sump. The affected piping was removed and associated piping/appurtenances were blinded. The failed pipe was sent for metallurgical analysis and it was determined that the cause was microbial induced, internal corrosion. New strainer piping installed will have an internal liner to prevent recurrence of internal corrosion and future releases.

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