HL incident on 2016-06-02 — TX

Operator
Kinder Morgan Wink Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5
Incident datetime
2016-06-02 09:45
Report number
Location
TX
Narrative
On 6/2/16, a kinder morgan employee was performing safety checks at kinder morgan's guadalupe station. The employee discovered a leak on the 1/2" tubing of the fitting on the cooling line for the pump outboard bearing box. The leak was contained within the pump building. Ferrules were removed from the tubing, and it was determined that the threads were worn on the nut and tubing fitting. The fitting and tubing were replaced.
Detailed record list
Report Received Date
2016-06-30 00:00:00
Iyear
2016
Report Number
20160208
Supplemental Number
21485
Report Type
Original
Operator Id
Name
Kinder Morgan Wink Pipeline Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-06-02 09:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.29
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-06-02 09:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-06-02 09:45:00
Restart Datetime
2016-06-02 14:15:00
On Site Datetime
2016-06-02 09:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Guadalupe Pump Station
Segment Name
20" Wink To Guadalupe
Onshore State Abbreviation
Tx
Onshore Postal Code
79847
Onshore City Name
Pine Springs
Onshore County Name
Culberson
Designated Location
Milepost/valve Station
Designated Name
Mp 113
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
13
Est Cost Prop Damage
5
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
18
Accident Psig
610
Mop Psig
650
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller does not see the fitting through scada. No alarms were received in the control center.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Vibration Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear At Threads From Repeatedly Removing And Re-Installing For Maintenance
Preparer Name
A**** Z*****
Preparer Title
Manager-Regulatory Compliance
Preparer Email
A***********@k***********.com
Preparer Telephone
713-369-9512
Preparer Fax
303-984-3417
Prepared Date
2016-06-30 00:00:00
Authorizer Name
S**** M*****
Authorizer Telephone
713-369-8065
Authorizer Title
Director-Operations And Engineering
Authorizer Email
S***********@k***********.com
Narrative
On 6/2/16, a kinder morgan employee was performing safety checks at kinder morgan's guadalupe station. The employee discovered a leak on the 1/2" tubing of the fitting on the cooling line for the pump outboard bearing box. The leak was contained within the pump building. Ferrules were removed from the tubing, and it was determined that the threads were worn on the nut and tubing fitting. The fitting and tubing were replaced.
Report Received Date 2016-06-30 00:00:00
Iyear 2016
Report Number 20160208
Supplemental Number 21485
Report Type Original
Operator Id 31957 PHMSA Enforcement
Name Kinder Morgan Wink Pipeline Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-06-02 09:45:00
Location Latitude 31.852417 Google Maps OpenStreetMap
Location Longitude -104.557182 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.29
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-06-02 09:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-06-02 09:45:00
Restart Datetime 2016-06-02 14:15:00
On Site Datetime 2016-06-02 09:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Guadalupe Pump Station
Segment Name 20" Wink To Guadalupe
Onshore State Abbreviation Tx
Onshore Postal Code 79847
Onshore City Name Pine Springs
Onshore County Name Culberson
Designated Location Milepost/valve Station
Designated Name Mp 113
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 13
Est Cost Prop Damage 5
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 18
Accident Psig 610
Mop Psig 650
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller does not see the fitting through scada. No alarms were received in the control center.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Vibration Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Wear At Threads From Repeatedly Removing And Re-Installing For Maintenance
Preparer Name A**** Z*****
Preparer Title Manager-Regulatory Compliance
Preparer Email A***********@k***********.com
Preparer Telephone 713-369-9512
Preparer Fax 303-984-3417
Prepared Date 2016-06-30 00:00:00
Authorizer Name S**** M*****
Authorizer Telephone 713-369-8065
Authorizer Title Director-Operations And Engineering
Authorizer Email S***********@k***********.com
Narrative On 6/2/16, a kinder morgan employee was performing safety checks at kinder morgan's guadalupe station. The employee discovered a leak on the 1/2" tubing of the fitting on the cooling line for the pump outboard bearing box. The leak was contained within the pump building. Ferrules were removed from the tubing, and it was determined that the threads were worn on the nut and tubing fitting. The fitting and tubing were replaced.

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