HL incident on 2016-05-31 — TX

Operator
Tesoro Socal Pipeline Company Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$191,869
Incident datetime
2016-05-31 07:40
Report number
Location
TX
Narrative
At approximately 7:40 a.M., a release of crude oil was discovered by an operator during his rounds of the carson crude terminal, which is an unmanned facility. The release appeared to be coming from a pipeline casing vent and was estimated at approximately 15 bbls. Three pipelines are in this area, so all three pipelines were shut down. The spill was released to the surrounding asphalt pavement and flowed to a narrow culvert which drains to a concrete-lined rainwater retention pond. The pond was empty at the time and the spill was completely contained on site. There was no impact to storm drains, waterways, or wildlife, nor were there any injuries caused by the spill. The spill was cleaned up promptly. The segment that leaked was permanently disconnected, and the line was re-routed.
Detailed record list
Report Received Date
2016-06-30 00:00:00
Iyear
2016
Report Number
20160205
Supplemental Number
22515
Report Type
Supplemental Final
Operator Id
Name
Tesoro Socal Pipeline Company Llc
Operator Street Address
19100 Ridgewood Parkway
Operator City Name
San Antonio
Operator State Abbreviation
TX
Operator Postal Code
78259
Local Datetime
2016-05-31 07:40:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2016-05-31 07:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Shut Down.
On Site Datetime
2016-05-31 08:00:00
Nrc Rpt Datetime
2016-05-31 08:45:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Carson Crude Terminal
Segment Name
Line 63
Onshore State Abbreviation
Ca
Onshore Postal Code
90745
Onshore City Name
Carson
Onshore County Name
Los Angeles
Designated Location
Survey Station No.
Designated Name
26+10
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
Unknown
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Cased
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.219
Pipe Smys
52000
Pipe Specification
Api 5l X52
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Polyolefin
Installation Year
1978
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
675
Est Cost Prop Damage
191869
Est Cost Emergency
175000
Est Cost Environmental
14980
Est Cost Other
0
Prpty
382524
Accident Psig
70
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
2078
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Other Inspection Ind
Yes
Internal Inspection Details
No Launchers Or Receivers.
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
The Line Was Abandoned In Place Without Examination. So, This Is Based On Analysis Of The Previous History Of This Line.
Int Other Loc Ind
Yes
Corrosion Location Details
Dead Leg
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2013
Hydrtst Most Rcnt Pressure
1097
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
H**** M****
Preparer Title
Senior Regulatory Compliance Specialist
Preparer Email
H************@t******.com
Preparer Telephone
210-626-4901
Prepared Date
2017-07-31 00:00:00
Authorizer Name
A**** M*******
Authorizer Telephone
210-626-6343
Authorizer Title
Director Compliance-Logistics
Authorizer Email
A***************@t******.com
Narrative
At approximately 7:40 a.M., a release of crude oil was discovered by an operator during his rounds of the carson crude terminal, which is an unmanned facility. The release appeared to be coming from a pipeline casing vent and was estimated at approximately 15 bbls. Three pipelines are in this area, so all three pipelines were shut down. The spill was released to the surrounding asphalt pavement and flowed to a narrow culvert which drains to a concrete-lined rainwater retention pond. The pond was empty at the time and the spill was completely contained on site. There was no impact to storm drains, waterways, or wildlife, nor were there any injuries caused by the spill. The spill was cleaned up promptly. The segment that leaked was permanently disconnected, and the line was re-routed.
Report Received Date 2016-06-30 00:00:00
Iyear 2016
Report Number 20160205
Supplemental Number 22515
Report Type Supplemental Final
Operator Id 39013 PHMSA Enforcement
Name Tesoro Socal Pipeline Company Llc
Operator Street Address 19100 Ridgewood Parkway
Operator City Name San Antonio
Operator State Abbreviation TX
Operator Postal Code 78259
Local Datetime 2016-05-31 07:40:00
Location Latitude 33.80313 Google Maps OpenStreetMap
Location Longitude -118.252843 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2016-05-31 07:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Shut Down.
On Site Datetime 2016-05-31 08:00:00
Nrc Rpt Datetime 2016-05-31 08:45:00
Nrc Rpt Num 1149257 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Carson Crude Terminal
Segment Name Line 63
Onshore State Abbreviation Ca
Onshore Postal Code 90745
Onshore City Name Carson
Onshore County Name Los Angeles
Designated Location Survey Station No.
Designated Name 26+10
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover Unknown
Crossing Yes
Road Crossing Ind Yes
Road Type Cased
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.219
Pipe Smys 52000
Pipe Specification Api 5l X52
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Polyolefin
Installation Year 1978
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 675
Est Cost Prop Damage 191869
Est Cost Emergency 175000
Est Cost Environmental 14980
Est Cost Other 0
Prpty 382524
Accident Psig 70
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 2078
Internal Inspection Ind No
Tight Mitered Ind Yes
Other Inspection Ind Yes
Internal Inspection Details No Launchers Or Receivers.
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Water Acid Ind Yes
Int Microbiological Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details The Line Was Abandoned In Place Without Examination. So, This Is Based On Analysis Of The Previous History Of This Line.
Int Other Loc Ind Yes
Corrosion Location Details Dead Leg
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2013
Hydrtst Most Rcnt Pressure 1097
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name H**** M****
Preparer Title Senior Regulatory Compliance Specialist
Preparer Email H************@t******.com
Preparer Telephone 210-626-4901
Prepared Date 2017-07-31 00:00:00
Authorizer Name A**** M*******
Authorizer Telephone 210-626-6343
Authorizer Title Director Compliance-Logistics
Authorizer Email A***************@t******.com
Narrative At approximately 7:40 a.M., a release of crude oil was discovered by an operator during his rounds of the carson crude terminal, which is an unmanned facility. The release appeared to be coming from a pipeline casing vent and was estimated at approximately 15 bbls. Three pipelines are in this area, so all three pipelines were shut down. The spill was released to the surrounding asphalt pavement and flowed to a narrow culvert which drains to a concrete-lined rainwater retention pond. The pond was empty at the time and the spill was completely contained on site. There was no impact to storm drains, waterways, or wildlife, nor were there any injuries caused by the spill. The spill was cleaned up promptly. The segment that leaked was permanently disconnected, and the line was re-routed.

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