HL incident on 2016-06-02 — PA

Operator
West Shore Pipeline Co
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2016-06-02 14:29
Report number
Location
PA
Narrative
While delivering through harlem station a vapor alarm activated and shut down the pipeline. A pipeliner was on site and found that 20 gallons of gasoline had been released from the sump. The local osro was contacted and the affected gravel area around the sump was cleaned up. The product did not leave the property. The investigation is ongoing. 60 yards of soil was removed. On completion on a maintenance activity a drain valve was left open to the station sump. When the line was restarted the sump began to fill.
Detailed record list
Report Received Date
2016-06-24 00:00:00
Iyear
2016
Report Number
20160196
Supplemental Number
21831
Report Type
Supplemental Final
Operator Id
Name
West Shore Pipeline Co
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevard
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2016-06-02 14:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.48
Recovered Bbls
0.48
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2016-06-02 14:29:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-06-02 14:20:00
Restart Datetime
2016-06-02 18:40:00
On Site Datetime
2016-06-02 14:29:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Harlem Station
Segment Name
He
Onshore State Abbreviation
Il
Onshore Postal Code
60402
Onshore City Name
Forest View
Onshore County Name
Cook
Designated Location
Milepost/valve Station
Designated Name
He
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
10000
Est Cost Emergency
15000
Est Cost Environmental
0
Est Cost Other
0
Prpty
25060
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
M***** E*****
Preparer Title
Senior District Compliance Specialist
Preparer Email
M******@b******.com
Preparer Telephone
2197968230
Prepared Date
2016-11-14 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
6109044113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
While delivering through harlem station a vapor alarm activated and shut down the pipeline. A pipeliner was on site and found that 20 gallons of gasoline had been released from the sump. The local osro was contacted and the affected gravel area around the sump was cleaned up. The product did not leave the property. The investigation is ongoing. 60 yards of soil was removed. On completion on a maintenance activity a drain valve was left open to the station sump. When the line was restarted the sump began to fill.
Report Received Date 2016-06-24 00:00:00
Iyear 2016
Report Number 20160196
Supplemental Number 21831
Report Type Supplemental Final
Operator Id 22430 PHMSA Enforcement
Name West Shore Pipeline Co
Operator Street Address The Buckeye Building 6161 Hamilton Boulevard
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2016-06-02 14:20:00
Location Latitude 41.801632 Google Maps OpenStreetMap
Location Longitude -87.795604 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.48
Recovered Bbls 0.48
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2016-06-02 14:29:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-06-02 14:20:00
Restart Datetime 2016-06-02 18:40:00
On Site Datetime 2016-06-02 14:29:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Harlem Station
Segment Name He
Onshore State Abbreviation Il
Onshore Postal Code 60402
Onshore City Name Forest View
Onshore County Name Cook
Designated Location Milepost/valve Station
Designated Name He
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 10000
Est Cost Emergency 15000
Est Cost Environmental 0
Est Cost Other 0
Prpty 25060
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name M***** E*****
Preparer Title Senior District Compliance Specialist
Preparer Email M******@b******.com
Preparer Telephone 2197968230
Prepared Date 2016-11-14 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 6109044113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative While delivering through harlem station a vapor alarm activated and shut down the pipeline. A pipeliner was on site and found that 20 gallons of gasoline had been released from the sump. The local osro was contacted and the affected gravel area around the sump was cleaned up. The product did not leave the property. The investigation is ongoing. 60 yards of soil was removed. On completion on a maintenance activity a drain valve was left open to the station sump. When the line was restarted the sump began to fill.

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