HL incident on 2016-05-27 — TX

Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2016-05-27 13:15
Report number
Location
TX
Narrative
On friday, 5/27/2016 at 13:04, a high-high lel alarm condition triggered a facility lockout at twin oaks meter station and pieline shut down. Event notification was sent to supervision and field personnel were dispatched to investigate. Leak was discovered at the receiving pig trap door. Response included isolation of the pig trap and flaring of the remaining product contained in the pig trap. When purged and made safe to open, the pig trap door was assessed and it was determined that the o-ring door seal had failed which caused the release. A new o-ring was installed, leak tested and the pipeline was returned to normal operation.
Detailed record list
Report Received Date
2016-06-22 00:00:00
Iyear
2016
Report Number
20160192
Supplemental Number
21777
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-05-27 13:04:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
9.1
Intentional Release Bbls
1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2016-05-27 13:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-05-27 13:04:00
Restart Datetime
2016-05-27 17:26:00
On Site Datetime
2016-05-27 13:55:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Tw14-Twin Oaks Meter Station
Segment Name
11190-8" Twin Oaks To Montello
Onshore State Abbreviation
Pa
Onshore Postal Code
19014
Onshore City Name
Aston
Onshore County Name
Delaware
Designated Location
Milepost/valve Station
Designated Name
Twin Oaks
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Viton O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
123
Est Cost Prop Damage
50
Est Cost Emergency
7570
Est Cost Environmental
0
Est Cost Other
0
Prpty
7743
Accident Psig
1102
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
O-Ring Failed.
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-10-20 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s*************.com
Narrative
On friday, 5/27/2016 at 13:04, a high-high lel alarm condition triggered a facility lockout at twin oaks meter station and pieline shut down. Event notification was sent to supervision and field personnel were dispatched to investigate. Leak was discovered at the receiving pig trap door. Response included isolation of the pig trap and flaring of the remaining product contained in the pig trap. When purged and made safe to open, the pig trap door was assessed and it was determined that the o-ring door seal had failed which caused the release. A new o-ring was installed, leak tested and the pipeline was returned to normal operation.
Report Received Date 2016-06-22 00:00:00
Iyear 2016
Report Number 20160192
Supplemental Number 21777
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-05-27 13:04:00
Location Latitude 39.844773 Google Maps OpenStreetMap
Location Longitude -75.418525 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 9.1
Intentional Release Bbls 1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2016-05-27 13:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-05-27 13:04:00
Restart Datetime 2016-05-27 17:26:00
On Site Datetime 2016-05-27 13:55:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Tw14-Twin Oaks Meter Station
Segment Name 11190-8" Twin Oaks To Montello
Onshore State Abbreviation Pa
Onshore Postal Code 19014
Onshore City Name Aston
Onshore County Name Delaware
Designated Location Milepost/valve Station
Designated Name Twin Oaks
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Viton O-Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 123
Est Cost Prop Damage 50
Est Cost Emergency 7570
Est Cost Environmental 0
Est Cost Other 0
Prpty 7743
Accident Psig 1102
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details O-Ring Failed.
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-10-20 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s*************.com
Narrative On friday, 5/27/2016 at 13:04, a high-high lel alarm condition triggered a facility lockout at twin oaks meter station and pieline shut down. Event notification was sent to supervision and field personnel were dispatched to investigate. Leak was discovered at the receiving pig trap door. Response included isolation of the pig trap and flaring of the remaining product contained in the pig trap. When purged and made safe to open, the pig trap door was assessed and it was determined that the o-ring door seal had failed which caused the release. A new o-ring was installed, leak tested and the pipeline was returned to normal operation.

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