HL incident on 2016-05-23 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2016-05-23 19:48
Report number
Location
OK
Narrative
Oneok pipeline controls center received a call from local emergency response team at 19:48, which had responded to a 911 call from the public regarding vapors coming from a pipeline valve. Pipeline control center shutdown pipeline and contacted oneok pipeline supervisor and local field representative. Local representative arrived onsite at 20:54 and identified vapors coming from the valve stem packing. Valve stem was packed with new packing and release stopped at 21:46. Oneok pipeline control center restarted pipeline and oneok representative remained onsite until line was back to full operation pressure to insure packing had stopped the release.
Detailed record list
Report Received Date
2016-06-21 00:00:00
Iyear
2016
Report Number
20160191
Supplemental Number
21453
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2016-05-23 19:48:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.16
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2016-05-23 19:48:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-05-23 19:48:00
Restart Datetime
2016-05-23 21:46:00
On Site Datetime
2016-05-23 20:54:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Oneok Sterling 1 Pipeline
Segment Name
Oneok Index # 10177
Onshore State Abbreviation
Tx
Onshore Postal Code
77327
Onshore City Name
Not Within A Municipality
Onshore County Name
Liberty
Designated Location
Milepost/valve Station
Designated Name
8736+64
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
M & J 303
Installation Year
1981
Manufactured Year
1981
Material Involved
Material Other Than Carbon Steel
Material Details
Valve Stem Packing
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7
Est Cost Prop Damage
50
Est Cost Emergency
150
Est Cost Environmental
0
Est Cost Other
0
Prpty
207
Accident Psig
842
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Vapor release was reported from valve by public and no controller actions had taken place to affect the pipeline
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Failure Of Valve Stem Packing
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2016-06-21 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
Oneok pipeline controls center received a call from local emergency response team at 19:48, which had responded to a 911 call from the public regarding vapors coming from a pipeline valve. Pipeline control center shutdown pipeline and contacted oneok pipeline supervisor and local field representative. Local representative arrived onsite at 20:54 and identified vapors coming from the valve stem packing. Valve stem was packed with new packing and release stopped at 21:46. Oneok pipeline control center restarted pipeline and oneok representative remained onsite until line was back to full operation pressure to insure packing had stopped the release.
Report Received Date 2016-06-21 00:00:00
Iyear 2016
Report Number 20160191
Supplemental Number 21453
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2016-05-23 19:48:00
Location Latitude 30.314425 Google Maps OpenStreetMap
Location Longitude -95.016202 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.16
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2016-05-23 19:48:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-05-23 19:48:00
Restart Datetime 2016-05-23 21:46:00
On Site Datetime 2016-05-23 20:54:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Oneok Sterling 1 Pipeline
Segment Name Oneok Index # 10177
Onshore State Abbreviation Tx
Onshore Postal Code 77327
Onshore City Name Not Within A Municipality
Onshore County Name Liberty
Designated Location Milepost/valve Station
Designated Name 8736+64
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer M & J 303
Installation Year 1981
Manufactured Year 1981
Material Involved Material Other Than Carbon Steel
Material Details Valve Stem Packing
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7
Est Cost Prop Damage 50
Est Cost Emergency 150
Est Cost Environmental 0
Est Cost Other 0
Prpty 207
Accident Psig 842
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Vapor release was reported from valve by public and no controller actions had taken place to affect the pipeline
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Failure Of Valve Stem Packing
Preparer Name N*** J****
Preparer Title Regulatory Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2016-06-21 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative Oneok pipeline controls center received a call from local emergency response team at 19:48, which had responded to a 911 call from the public regarding vapors coming from a pipeline valve. Pipeline control center shutdown pipeline and contacted oneok pipeline supervisor and local field representative. Local representative arrived onsite at 20:54 and identified vapors coming from the valve stem packing. Valve stem was packed with new packing and release stopped at 21:46. Oneok pipeline control center restarted pipeline and oneok representative remained onsite until line was back to full operation pressure to insure packing had stopped the release.

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