HL incident on 2016-05-16 — OK

Operator
Magellan Terminals Holdings, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-05-16 06:10
Report number
Location
OK
Narrative
Following receipt of an inbound delivery into tank 388, a local operator entered the tank containment to close the incoming valve of tank 388 and discovered product coming out of a bleeder valve on the transfer pump discharge. The valve was closed and product recovered. Impacted soil will be remediated.
Detailed record list
Report Received Date
2016-06-14 00:00:00
Iyear
2016
Report Number
20160182
Supplemental Number
21438
Report Type
Original Final
Operator Id
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2016-05-16 06:10:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
38
Recovered Bbls
38
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-05-16 06:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Idle At The Time Of Discovery
On Site Datetime
2016-05-16 06:10:00
Nrc Rpt Datetime
2016-05-16 07:01:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal
Segment Name
Terminal No. 474, Tank No. 388 Auxiliary Tank Pump
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Bleeder Valve On Auxiliary Pump
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Bleeder Valve Left Open Following Delivery Into Tank 388
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1300
Est Cost Prop Damage
0
Est Cost Emergency
8000
Est Cost Environmental
7500
Est Cost Other
0
Prpty
16800
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Bleeder Valve On Discharge Side Of Auxiliary Stripper Pump Was Left Open With Plug Removed Causing Product To Come Out Of The Bleeder Valve.
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K****** L* L*******
Preparer Title
Senior Compliance Coordinator
Preparer Email
No Email Address
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2016-06-14 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Senior Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Following receipt of an inbound delivery into tank 388, a local operator entered the tank containment to close the incoming valve of tank 388 and discovered product coming out of a bleeder valve on the transfer pump discharge. The valve was closed and product recovered. Impacted soil will be remediated.
Report Received Date 2016-06-14 00:00:00
Iyear 2016
Report Number 20160182
Supplemental Number 21438
Report Type Original Final
Operator Id 31580 PHMSA Enforcement
Name Magellan Terminals Holdings, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2016-05-16 06:10:00
Location Latitude 29.7474 Google Maps OpenStreetMap
Location Longitude -95.20457 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 38
Recovered Bbls 38
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-05-16 06:10:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Idle At The Time Of Discovery
On Site Datetime 2016-05-16 06:10:00
Nrc Rpt Datetime 2016-05-16 07:01:00
Nrc Rpt Num 1147850 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Galena Park Terminal
Segment Name Terminal No. 474, Tank No. 388 Auxiliary Tank Pump
Onshore State Abbreviation Tx
Onshore Postal Code 77547
Onshore City Name Galena Park
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Bleeder Valve On Auxiliary Pump
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2016
Material Involved Carbon Steel
Release Type Other
Release Type Details Bleeder Valve Left Open Following Delivery Into Tank 388
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1300
Est Cost Prop Damage 0
Est Cost Emergency 8000
Est Cost Environmental 7500
Est Cost Other 0
Prpty 16800
Accident Psig 50
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Bleeder Valve On Discharge Side Of Auxiliary Stripper Pump Was Left Open With Plug Removed Causing Product To Come Out Of The Bleeder Valve.
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name K****** L* L*******
Preparer Title Senior Compliance Coordinator
Preparer Email No Email Address
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2016-06-14 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Senior Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative Following receipt of an inbound delivery into tank 388, a local operator entered the tank containment to close the incoming valve of tank 388 and discovered product coming out of a bleeder valve on the transfer pump discharge. The valve was closed and product recovered. Impacted soil will be remediated.

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