Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2016-05-16 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2016-05-16 06:10
Report number
Location
OK
Narrative
Following receipt of an inbound delivery into tank 388, a local operator entered the tank containment to close the incoming valve of tank 388 and discovered product coming out of a bleeder valve on the transfer pump discharge. The valve was closed and product recovered. Impacted soil will be remediated.
Detailed record list
Report Received Date
2016-06-14 00:00:00
Iyear
2016
Report Number
20160182
Supplemental Number
21438
Report Type
Original Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2016-05-16 06:10:00
Location Latitude
29.7474
Location Longitude
-95.20457
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
38
Recovered Bbls
38
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-05-16 06:10:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Idle At The Time Of Discovery
On Site Datetime
2016-05-16 06:10:00
Nrc Rpt Datetime
2016-05-16 07:01:00
Nrc Rpt Num
1147850
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal
Segment Name
Terminal No. 474, Tank No. 388 Auxiliary Tank Pump
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Bleeder Valve On Auxiliary Pump
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2016
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Bleeder Valve Left Open Following Delivery Into Tank 388
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1300
Est Cost Prop Damage
0
Est Cost Emergency
8000
Est Cost Environmental
7500
Est Cost Other
0
Prpty
16800
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Bleeder Valve On Discharge Side Of Auxiliary Stripper Pump Was Left Open With Plug Removed Causing Product To Come Out Of The Bleeder Valve.
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
K****** L* L*******
Preparer Title
Senior Compliance Coordinator
Preparer Email
No Email Address
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2016-06-14 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Senior Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Following receipt of an inbound delivery into tank 388, a local operator entered the tank containment to close the incoming valve of tank 388 and discovered product coming out of a bleeder valve on the transfer pump discharge. The valve was closed and product recovered. Impacted soil will be remediated.
| Report Received Date | 2016-06-14 00:00:00 |
|---|---|
| Iyear | 2016 |
| Report Number | 20160182 |
| Supplemental Number | 21438 |
| Report Type | Original Final |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2016-05-16 06:10:00 |
| Location Latitude | 29.7474 Google Maps OpenStreetMap |
| Location Longitude | -95.20457 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 38 |
| Recovered Bbls | 38 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2016-05-16 06:10:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Line Was Idle At The Time Of Discovery |
| On Site Datetime | 2016-05-16 06:10:00 |
| Nrc Rpt Datetime | 2016-05-16 07:01:00 |
| Nrc Rpt Num | 1147850 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Galena Park Terminal |
| Segment Name | Terminal No. 474, Tank No. 388 Auxiliary Tank Pump |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77547 |
| Onshore City Name | Galena Park |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Other |
| Incident Area Details | Bleeder Valve On Auxiliary Pump |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Valve |
| Valve Type | Auxiliary Or Other Valve |
| Installation Year | 2016 |
| Material Involved | Carbon Steel |
| Release Type | Other |
| Release Type Details | Bleeder Valve Left Open Following Delivery Into Tank 388 |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 1300 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 8000 |
| Est Cost Environmental | 7500 |
| Est Cost Other | 0 |
| Prpty | 16800 |
| Accident Psig | 50 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Other Incorrect Operation |
| Operation Type | Other Incorrect Operation |
| Operation Details | Bleeder Valve On Discharge Side Of Auxiliary Stripper Pump Was Left Open With Plug Removed Causing Product To Come Out Of The Bleeder Valve. |
| Related Failure Follow Ind | Yes |
| Category Type | Normal Operating Conditions |
| Operator Qualification Ind | Yes |
| Qualified Individuals | Yes, They Were Qualified For The Task(S) |
| Preparer Name | K****** L* L******* |
| Preparer Title | Senior Compliance Coordinator |
| Preparer Email | No Email Address |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7377 |
| Prepared Date | 2016-06-14 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Senior Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | Following receipt of an inbound delivery into tank 388, a local operator entered the tank containment to close the incoming valve of tank 388 and discovered product coming out of a bleeder valve on the transfer pump discharge. The valve was closed and product recovered. Impacted soil will be remediated. |
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