HL incident on 2016-05-05 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2016-05-05 16:16
Report number
Location
TX
Narrative
On may 5th, 2016, at approximately 16:00 hrs energy transfer liquid control contacted company field personnel requesting assistance at the baden facility, due to increasing pressures. At 16:10 hrs, energy transfer employee, on location at baden facility, heard a relief valve activate on a 10" stationary meter prover. The employee notified liquid control that baden was being over pressured and to reroute incoming product. At 16:16 hrs, the flange gasket failed on the 10" stationary meter prover, resulting in a release of product. Liquid control was notified to shut down baden facility. The 10" stationary meter prover loop was shut down and isolated, the gasket was replaced and the facility was returned to service at 22:40 hrs. The product released was estimated at 63 bbls. This facility is under jurisdiction of the texas railroad commission and were telephonically notified of the release under report number 1348. Preliminary investigations have revealed that a third party delivery had inadvertently increased flow, into the baden facility, and station equipment was unable to react quick enough to prevent the over pressuring. The inlet piping was modified on may 21, 2016 so that there is adequate protection and reoccurrence is not possible. Update 11/29/2016 no updates to be made. Note as final report.
Detailed record list
Report Received Date
2016-06-03 00:00:00
Iyear
2016
Report Number
20160169
Supplemental Number
21893
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-05-05 16:16:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
63
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-05-05 16:16:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-05-05 16:39:00
Restart Datetime
2016-05-05 22:40:00
On Site Datetime
2016-05-05 16:16:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Baden Underground Storage
Segment Name
10" Stationary Prover Loop
Onshore State Abbreviation
Tx
Onshore Postal Code
79782
Onshore City Name
Not Within A Municipality
Onshore County Name
Martin
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Installation Year
1974
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket Material
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1008
Est Cost Prop Damage
100
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1108
Accident Psig
1023
Mop Psig
720
Accident Pressure
Pressure Exceeded 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller immediately identified the overpressure condition and shut down the facility. The controllers actions were appropriate for the events that occurred. No investigation is necessary.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Control Valve Ind
Yes
Additional Overpressure Ind
Yes
Preparer Name
D**** N******
Preparer Title
Director Regulatory Compliance
Preparer Email
D************@e*************.com
Preparer Telephone
713-989-7232
Prepared Date
2016-11-29 00:00:00
Authorizer Name
D**** N******
Authorizer Telephone
713-989-7232
Authorizer Title
Director Regulatory Compliance
Authorizer Email
D************@e*************.com
Narrative
On may 5th, 2016, at approximately 16:00 hrs energy transfer liquid control contacted company field personnel requesting assistance at the baden facility, due to increasing pressures. At 16:10 hrs, energy transfer employee, on location at baden facility, heard a relief valve activate on a 10" stationary meter prover. The employee notified liquid control that baden was being over pressured and to reroute incoming product. At 16:16 hrs, the flange gasket failed on the 10" stationary meter prover, resulting in a release of product. Liquid control was notified to shut down baden facility. The 10" stationary meter prover loop was shut down and isolated, the gasket was replaced and the facility was returned to service at 22:40 hrs. The product released was estimated at 63 bbls. This facility is under jurisdiction of the texas railroad commission and were telephonically notified of the release under report number 1348. Preliminary investigations have revealed that a third party delivery had inadvertently increased flow, into the baden facility, and station equipment was unable to react quick enough to prevent the over pressuring. The inlet piping was modified on may 21, 2016 so that there is adequate protection and reoccurrence is not possible. Update 11/29/2016 no updates to be made. Note as final report.
Report Received Date 2016-06-03 00:00:00
Iyear 2016
Report Number 20160169
Supplemental Number 21893
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-05-05 16:16:00
Location Latitude 32.090307 Google Maps OpenStreetMap
Location Longitude -101.8809 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 63
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-05-05 16:16:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-05-05 16:39:00
Restart Datetime 2016-05-05 22:40:00
On Site Datetime 2016-05-05 16:16:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Baden Underground Storage
Segment Name 10" Stationary Prover Loop
Onshore State Abbreviation Tx
Onshore Postal Code 79782
Onshore City Name Not Within A Municipality
Onshore County Name Martin
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Meter/prover
Installation Year 1974
Material Involved Material Other Than Carbon Steel
Material Details Gasket Material
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1008
Est Cost Prop Damage 100
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1108
Accident Psig 1023
Mop Psig 720
Accident Pressure Pressure Exceeded 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller immediately identified the overpressure condition and shut down the facility. The controllers actions were appropriate for the events that occurred. No investigation is necessary.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Control Valve Ind Yes
Additional Overpressure Ind Yes
Preparer Name D**** N******
Preparer Title Director Regulatory Compliance
Preparer Email D************@e*************.com
Preparer Telephone 713-989-7232
Prepared Date 2016-11-29 00:00:00
Authorizer Name D**** N******
Authorizer Telephone 713-989-7232
Authorizer Title Director Regulatory Compliance
Authorizer Email D************@e*************.com
Narrative On may 5th, 2016, at approximately 16:00 hrs energy transfer liquid control contacted company field personnel requesting assistance at the baden facility, due to increasing pressures. At 16:10 hrs, energy transfer employee, on location at baden facility, heard a relief valve activate on a 10" stationary meter prover. The employee notified liquid control that baden was being over pressured and to reroute incoming product. At 16:16 hrs, the flange gasket failed on the 10" stationary meter prover, resulting in a release of product. Liquid control was notified to shut down baden facility. The 10" stationary meter prover loop was shut down and isolated, the gasket was replaced and the facility was returned to service at 22:40 hrs. The product released was estimated at 63 bbls. This facility is under jurisdiction of the texas railroad commission and were telephonically notified of the release under report number 1348. Preliminary investigations have revealed that a third party delivery had inadvertently increased flow, into the baden facility, and station equipment was unable to react quick enough to prevent the over pressuring. The inlet piping was modified on may 21, 2016 so that there is adequate protection and reoccurrence is not possible. Update 11/29/2016 no updates to be made. Note as final report.

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