HL incident on 2016-05-05 — TX

Operator
Energy Transfer Company
Cause
Other Accident Cause
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-05-05 15:15
Report number
Location
TX
Narrative
On may 5th at approximately 15:15 hrs. Energy transfer liquids control identified an overpressure condition on energy transfer's lone star west texas gateway 16in. Ngl pipeline. The liquids controller immediately shut down the pipeline and contacted an operations technician that was working at one of the pump stations on the system. The operations technician verified the condition and notified the controller that thermal relief valves were venting at three different facilities, along the pipeline. Liquids control was notified that one of the downstream facilities accepting product from this system inadvertently shut in, causing this condition. No damages resulted and the condition was resolved after a 24 minute outage. The system was brought back into service at 15:39 hrs. On may 5th.
Detailed record list
Report Received Date
2016-05-31 00:00:00
Iyear
2016
Report Number
20160161
Supplemental Number
21398
Report Type
Original Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-05-05 15:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
694
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2016-05-05 15:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-05-05 15:15:00
Restart Datetime
2016-05-05 15:39:00
On Site Datetime
2016-05-05 15:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
West Texas Gateway 16in
Segment Name
Pump Station # 3
Onshore State Abbreviation
Tx
Onshore Postal Code
76943
Onshore City Name
Ozona
Onshore County Name
Crockett
Designated Location
Milepost/valve Station
Designated Name
92.2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
11104
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
11104
Accident Psig
1567
Mop Psig
1440
Accident Pressure
Pressure Exceeded Mop, But Did Not Exceed 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller immediately identified the overpressure condition and shut down the pipeline. The controllers actions were appropriate for the events that occurred. No investigation is necessary.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
A Facility Downstream Of This Pipeline Had Operational Issues And Inadvertently Shut In, Causing This Pipeline And Other Facilities Upstream And Downstream Of This System To Immediately Loose Outlet Flow Capability. This Pipeline Over Pressured And Vented Product At One Of The Pigging Facilities Before The System Could Be Returned To Normal Operating Parameters.
Preparer Name
D**** N******
Preparer Title
Director Regulatory Compliance
Preparer Email
D************@e*************.com
Preparer Telephone
713.989.7232
Prepared Date
2016-05-31 00:00:00
Authorizer Name
D**** N******
Authorizer Telephone
7139897232
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
D************@e*************.com
Narrative
On may 5th at approximately 15:15 hrs. Energy transfer liquids control identified an overpressure condition on energy transfer's lone star west texas gateway 16in. Ngl pipeline. The liquids controller immediately shut down the pipeline and contacted an operations technician that was working at one of the pump stations on the system. The operations technician verified the condition and notified the controller that thermal relief valves were venting at three different facilities, along the pipeline. Liquids control was notified that one of the downstream facilities accepting product from this system inadvertently shut in, causing this condition. No damages resulted and the condition was resolved after a 24 minute outage. The system was brought back into service at 15:39 hrs. On may 5th.
Report Received Date 2016-05-31 00:00:00
Iyear 2016
Report Number 20160161
Supplemental Number 21398
Report Type Original Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-05-05 15:15:00
Location Latitude 30.684 Google Maps OpenStreetMap
Location Longitude -101.27111 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 694
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2016-05-05 15:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-05-05 15:15:00
Restart Datetime 2016-05-05 15:39:00
On Site Datetime 2016-05-05 15:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name West Texas Gateway 16in
Segment Name Pump Station # 3
Onshore State Abbreviation Tx
Onshore Postal Code 76943
Onshore City Name Ozona
Onshore County Name Crockett
Designated Location Milepost/valve Station
Designated Name 92.2
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2012
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 11104
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 11104
Accident Psig 1567
Mop Psig 1440
Accident Pressure Pressure Exceeded Mop, But Did Not Exceed 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller immediately identified the overpressure condition and shut down the pipeline. The controllers actions were appropriate for the events that occurred. No investigation is necessary.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details A Facility Downstream Of This Pipeline Had Operational Issues And Inadvertently Shut In, Causing This Pipeline And Other Facilities Upstream And Downstream Of This System To Immediately Loose Outlet Flow Capability. This Pipeline Over Pressured And Vented Product At One Of The Pigging Facilities Before The System Could Be Returned To Normal Operating Parameters.
Preparer Name D**** N******
Preparer Title Director Regulatory Compliance
Preparer Email D************@e*************.com
Preparer Telephone 713.989.7232
Prepared Date 2016-05-31 00:00:00
Authorizer Name D**** N******
Authorizer Telephone 7139897232
Authorizer Title Director - Regulatory Compliance
Authorizer Email D************@e*************.com
Narrative On may 5th at approximately 15:15 hrs. Energy transfer liquids control identified an overpressure condition on energy transfer's lone star west texas gateway 16in. Ngl pipeline. The liquids controller immediately shut down the pipeline and contacted an operations technician that was working at one of the pump stations on the system. The operations technician verified the condition and notified the controller that thermal relief valves were venting at three different facilities, along the pipeline. Liquids control was notified that one of the downstream facilities accepting product from this system inadvertently shut in, causing this condition. No damages resulted and the condition was resolved after a 24 minute outage. The system was brought back into service at 15:39 hrs. On may 5th.

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