HL incident on 2016-04-28 — TX

Operator
Rose Rock Midstream L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$12,500
Incident datetime
2016-04-28 10:45
Report number
Location
TX
Narrative
4/18/2017 - updated anticipated remediation to yes, and that soil was remediated. 10:45 am on 4/28/2016, the aerial patrol pilot identified a leak in corn field. The aerial patrol pilot notified the maintenance supervisor who contacted the control center to immediate shut down hanston station. The maintenance supervisor drove to kaufman junction and closed block valve at 11:15 am. He then drove to hudson station and closed the downstream valve. A vac truck and backhoe were dispatched for remediation and to uncover the pipe. The pipe was uncovered at 14:00 and it was found the 8" pipe had an internal involved corrosion pinhole leak in the 7 o'clock position. On 5/2/16, we completed a 13' 9" pipe replacement with welds being coated. The pipeline was put back into service on 5/2/16 at 13:45. 7/19/2017 this report was corrected to show remediation was required and the associated remediation costs were updated
Detailed record list
Report Received Date
2016-05-26 00:00:00
Iyear
2016
Report Number
20160160
Supplemental Number
22487
Report Type
Supplemental Final
Operator Id
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-04-28 10:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2016-04-28 10:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-04-28 10:46:00
Restart Datetime
2016-05-02 13:45:00
On Site Datetime
2016-04-28 12:06:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Hanston Station
Segment Name
Hanston To Hudson 8"
Onshore State Abbreviation
Ks
Onshore Postal Code
67525
Onshore City Name
Not Within A Municipality
Onshore County Name
Stafford
Designated Location
Milepost/valve Station
Designated Name
10
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.322
Pipe Smys
24000
Pipe Specification
Api 5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
National
Pipe Coating Type
Coal Tar
Installation Year
1944
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
500
Est Cost Gas Released
60
Est Cost Prop Damage
12500
Est Cost Emergency
2500
Est Cost Environmental
9096
Est Cost Other
0
Prpty
24656
Accident Psig
37
Mop Psig
397
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
42240
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was an internal corrosion leak and the control center did not have any affect on this leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
700 Position
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
D**** Y****
Preparer Title
District Manager
Preparer Email
D******@s***********.com
Preparer Telephone
620-727-2173
Prepared Date
2017-07-19 00:00:00
Authorizer Name
T*** A*******
Authorizer Telephone
620-309-8101
Authorizer Title
Dot Compliance Manager
Authorizer Email
T********@s***********.com
Narrative
4/18/2017 - updated anticipated remediation to yes, and that soil was remediated. 10:45 am on 4/28/2016, the aerial patrol pilot identified a leak in corn field. The aerial patrol pilot notified the maintenance supervisor who contacted the control center to immediate shut down hanston station. The maintenance supervisor drove to kaufman junction and closed block valve at 11:15 am. He then drove to hudson station and closed the downstream valve. A vac truck and backhoe were dispatched for remediation and to uncover the pipe. The pipe was uncovered at 14:00 and it was found the 8" pipe had an internal involved corrosion pinhole leak in the 7 o'clock position. On 5/2/16, we completed a 13' 9" pipe replacement with welds being coated. The pipeline was put back into service on 5/2/16 at 13:45. 7/19/2017 this report was corrected to show remediation was required and the associated remediation costs were updated
Report Received Date 2016-05-26 00:00:00
Iyear 2016
Report Number 20160160
Supplemental Number 22487
Report Type Supplemental Final
Operator Id 31476 PHMSA Enforcement
Name Rose Rock Midstream L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-04-28 10:45:00
Location Latitude 38.093693 Google Maps OpenStreetMap
Location Longitude -98.682561 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2016-04-28 10:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-04-28 10:46:00
Restart Datetime 2016-05-02 13:45:00
On Site Datetime 2016-04-28 12:06:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Hanston Station
Segment Name Hanston To Hudson 8"
Onshore State Abbreviation Ks
Onshore Postal Code 67525
Onshore City Name Not Within A Municipality
Onshore County Name Stafford
Designated Location Milepost/valve Station
Designated Name 10
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.322
Pipe Smys 24000
Pipe Specification Api 5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer National
Pipe Coating Type Coal Tar
Installation Year 1944
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 500
Est Cost Gas Released 60
Est Cost Prop Damage 12500
Est Cost Emergency 2500
Est Cost Environmental 9096
Est Cost Other 0
Prpty 24656
Accident Psig 37
Mop Psig 397
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 42240
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was an internal corrosion leak and the control center did not have any affect on this leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details 700 Position
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name D**** Y****
Preparer Title District Manager
Preparer Email D******@s***********.com
Preparer Telephone 620-727-2173
Prepared Date 2017-07-19 00:00:00
Authorizer Name T*** A*******
Authorizer Telephone 620-309-8101
Authorizer Title Dot Compliance Manager
Authorizer Email T********@s***********.com
Narrative 4/18/2017 - updated anticipated remediation to yes, and that soil was remediated. 10:45 am on 4/28/2016, the aerial patrol pilot identified a leak in corn field. The aerial patrol pilot notified the maintenance supervisor who contacted the control center to immediate shut down hanston station. The maintenance supervisor drove to kaufman junction and closed block valve at 11:15 am. He then drove to hudson station and closed the downstream valve. A vac truck and backhoe were dispatched for remediation and to uncover the pipe. The pipe was uncovered at 14:00 and it was found the 8" pipe had an internal involved corrosion pinhole leak in the 7 o'clock position. On 5/2/16, we completed a 13' 9" pipe replacement with welds being coated. The pipeline was put back into service on 5/2/16 at 13:45. 7/19/2017 this report was corrected to show remediation was required and the associated remediation costs were updated

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