HL incident on 2016-04-24 — TX

Operator
Energy Transfer Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2016-04-24 11:35
Report number
Location
TX
Narrative
On april 24th at approximately 2335 hrs., buckeye operations notified energy transfer company's liquids control that there was a possible leak at the ef-90 meter station at the end of the rio bravo pipeline. Liquids control immediately shut down the pipeline and operations technician was dispatched to investigate. Etc operations arrived on site at approximately 0015 hrs. On april 25th and verified oil on the ground within the station. An inspection dig was conducted and the 8" pigging receiver bypass line was found to have a small hole. The segment of the line with the defect was removed and sent to a lab for testing. The line was replaced and brought back into service on 1600 hrs. On april 27th. This pipeline is under jurisdiction of the trrc as intrastate (system id 963373). Leak was telephonically reported to trrc on 04/25/2016, under report # 1344. Update 10/11/2016 upon receipt of metallurgical report, cause of release is confirmed as result of microbiological induced corrosion (mic).
Detailed record list
Report Received Date
2016-05-24 00:00:00
Iyear
2016
Report Number
20160156
Supplemental Number
21754
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-04-24 23:35:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Buckeye Plant Operator
Incident Identified Datetime
2016-04-24 11:35:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-04-24 11:35:00
Restart Datetime
2016-04-27 16:00:00
On Site Datetime
2016-04-25 00:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Rio Bravo Crude Pipeline
Segment Name
Ef-90/ Buckeye Terminal
Onshore State Abbreviation
Tx
Onshore Postal Code
78022
Onshore City Name
Corpus Christi
Onshore County Name
Nueces
Designated Location
Survey Station No.
Designated Name
139+32.6
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
At Meter Station At End Of Line
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
600
Est Cost Prop Damage
2500
Est Cost Emergency
500
Est Cost Environmental
23000
Est Cost Other
0
Prpty
26600
Accident Psig
240
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Only indication of leak was a small amount of liquid on the ground identified by buckeye operator. Controller made no error in operating pipeline or handling of incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
D**** N******
Preparer Title
Director Regulatory Compliance
Preparer Email
D************@e*************.com
Preparer Telephone
713.989.7232
Prepared Date
2016-10-11 00:00:00
Authorizer Name
D**** N******
Authorizer Telephone
7139897232
Authorizer Title
Director- Regulatory Compliance
Authorizer Email
D************@e*************.com
Narrative
On april 24th at approximately 2335 hrs., buckeye operations notified energy transfer company's liquids control that there was a possible leak at the ef-90 meter station at the end of the rio bravo pipeline. Liquids control immediately shut down the pipeline and operations technician was dispatched to investigate. Etc operations arrived on site at approximately 0015 hrs. On april 25th and verified oil on the ground within the station. An inspection dig was conducted and the 8" pigging receiver bypass line was found to have a small hole. The segment of the line with the defect was removed and sent to a lab for testing. The line was replaced and brought back into service on 1600 hrs. On april 27th. This pipeline is under jurisdiction of the trrc as intrastate (system id 963373). Leak was telephonically reported to trrc on 04/25/2016, under report # 1344. Update 10/11/2016 upon receipt of metallurgical report, cause of release is confirmed as result of microbiological induced corrosion (mic).
Report Received Date 2016-05-24 00:00:00
Iyear 2016
Report Number 20160156
Supplemental Number 21754
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-04-24 23:35:00
Location Latitude 27.8125 Google Maps OpenStreetMap
Location Longitude -97.5036 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Buckeye Plant Operator
Incident Identified Datetime 2016-04-24 11:35:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-04-24 11:35:00
Restart Datetime 2016-04-27 16:00:00
On Site Datetime 2016-04-25 00:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Rio Bravo Crude Pipeline
Segment Name Ef-90/ Buckeye Terminal
Onshore State Abbreviation Tx
Onshore Postal Code 78022
Onshore City Name Corpus Christi
Onshore County Name Nueces
Designated Location Survey Station No.
Designated Name 139+32.6
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details At Meter Station At End Of Line
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 600
Est Cost Prop Damage 2500
Est Cost Emergency 500
Est Cost Environmental 23000
Est Cost Other 0
Prpty 26600
Accident Psig 240
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Only indication of leak was a small amount of liquid on the ground identified by buckeye operator. Controller made no error in operating pipeline or handling of incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name D**** N******
Preparer Title Director Regulatory Compliance
Preparer Email D************@e*************.com
Preparer Telephone 713.989.7232
Prepared Date 2016-10-11 00:00:00
Authorizer Name D**** N******
Authorizer Telephone 7139897232
Authorizer Title Director- Regulatory Compliance
Authorizer Email D************@e*************.com
Narrative On april 24th at approximately 2335 hrs., buckeye operations notified energy transfer company's liquids control that there was a possible leak at the ef-90 meter station at the end of the rio bravo pipeline. Liquids control immediately shut down the pipeline and operations technician was dispatched to investigate. Etc operations arrived on site at approximately 0015 hrs. On april 25th and verified oil on the ground within the station. An inspection dig was conducted and the 8" pigging receiver bypass line was found to have a small hole. The segment of the line with the defect was removed and sent to a lab for testing. The line was replaced and brought back into service on 1600 hrs. On april 27th. This pipeline is under jurisdiction of the trrc as intrastate (system id 963373). Leak was telephonically reported to trrc on 04/25/2016, under report # 1344. Update 10/11/2016 upon receipt of metallurgical report, cause of release is confirmed as result of microbiological induced corrosion (mic).

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