HL incident on 2016-04-23 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$14,321
Incident datetime
2016-04-23 09:00
Report number
Location
TX
Narrative
On the morning of 4/23/2016 the controller contacted local operating personnel to investigate excessive sump run alarms at ranger station. Local pipeliner arrived at ranger station at approximately 09:30 and discovered pump #4 shaft seal leaking. The station was shut down and isolated. Pump unit #4 was isolated and blinded for repair. Contaminated soil was removed for onsite remediation.
Detailed record list
Report Received Date
2016-05-18 00:00:00
Iyear
2016
Report Number
20160150
Supplemental Number
21379
Report Type
Original Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-04-23 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-04-23 09:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-04-23 09:40:00
Restart Datetime
2016-04-27 08:39:00
On Site Datetime
2016-04-23 09:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wtg-Ranger Station
Segment Name
23010-26" Colorado City To Wortham
Onshore State Abbreviation
Tx
Onshore Postal Code
76470
Onshore City Name
Ranger
Onshore County Name
Eastland
Designated Location
Survey Station No.
Designated Name
17667+79
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Pump Shaft Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
14321
Est Cost Emergency
3500
Est Cost Environmental
4500
Est Cost Other
0
Prpty
22321
Accident Psig
315
Mop Psig
750
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Additional Alarm Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Malfunction Of Seal Pot Alarm/shutdown
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-05-18 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On the morning of 4/23/2016 the controller contacted local operating personnel to investigate excessive sump run alarms at ranger station. Local pipeliner arrived at ranger station at approximately 09:30 and discovered pump #4 shaft seal leaking. The station was shut down and isolated. Pump unit #4 was isolated and blinded for repair. Contaminated soil was removed for onsite remediation.
Report Received Date 2016-05-18 00:00:00
Iyear 2016
Report Number 20160150
Supplemental Number 21379
Report Type Original Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-04-23 09:00:00
Location Latitude 32.49829 Google Maps OpenStreetMap
Location Longitude -98.63621 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-04-23 09:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-04-23 09:40:00
Restart Datetime 2016-04-27 08:39:00
On Site Datetime 2016-04-23 09:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wtg-Ranger Station
Segment Name 23010-26" Colorado City To Wortham
Onshore State Abbreviation Tx
Onshore Postal Code 76470
Onshore City Name Ranger
Onshore County Name Eastland
Designated Location Survey Station No.
Designated Name 17667+79
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Pump Shaft Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 14321
Est Cost Emergency 3500
Est Cost Environmental 4500
Est Cost Other 0
Prpty 22321
Accident Psig 315
Mop Psig 750
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Additional Alarm Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Malfunction Of Seal Pot Alarm/shutdown
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-05-18 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On the morning of 4/23/2016 the controller contacted local operating personnel to investigate excessive sump run alarms at ranger station. Local pipeliner arrived at ranger station at approximately 09:30 and discovered pump #4 shaft seal leaking. The station was shut down and isolated. Pump unit #4 was isolated and blinded for repair. Contaminated soil was removed for onsite remediation.

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