HL incident on 2016-04-06 — TX

Operator
Kinder Morgan Wink Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2016-04-06 09:35
Report number
Location
TX
Narrative
On 4/6/2016, the wink station operations supervisor walked outside of the office and smelled a crude odor. He visually inspected the station, and discovered a leak on the fill line at tank 26. The supervisor isolated the line. The section of the line that failed was visually examined by a corrosion subject matter expert, and determined to be internal corrosion. The line has been sent for lab analysis. An isolation valve was installed on the line. The line will be drained when not in use.
Detailed record list
Report Received Date
2016-05-05 00:00:00
Iyear
2016
Report Number
20160139
Supplemental Number
21461
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Wink Pipeline Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2016-04-06 09:35:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2016-04-06 09:35:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2016-04-06 09:35:00
Restart Datetime
2016-04-13 08:30:00
On Site Datetime
2016-04-06 09:35:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wink Station
Segment Name
Tank 26 Fill Line
Onshore State Abbreviation
Tx
Onshore Postal Code
79789
Onshore City Name
Wink
Onshore County Name
Winkler
Designated Location
Milepost/valve Station
Designated Name
195
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.25
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Installation Year
1953
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
160
Est Cost Prop Damage
10000
Est Cost Emergency
0
Est Cost Environmental
13000
Est Cost Other
0
Prpty
23160
Accident Psig
16
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller is not able to see the tank fill line through scada, only the tank level. There were no scada indications of a leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Scale Buildup - Under Deposit Corrosion
Int Field Exam Basis Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Failure Analysis And Microbial Assay
Int Other Loc Ind
Yes
Corrosion Location Details
Flange Entry Into Tank, Transition Between Pipe And Flange At 6 O'clock Position
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
A**** Z*****
Preparer Title
Manager-Regulatory Compliance
Preparer Email
A***********@k***********.com
Preparer Telephone
713-369-9512
Preparer Fax
303-984-3417
Prepared Date
2016-06-24 00:00:00
Authorizer Name
S**** M*****
Authorizer Telephone
7133698065
Authorizer Title
Director-Operations And Engineering
Authorizer Email
S***********@k***********.com
Narrative
On 4/6/2016, the wink station operations supervisor walked outside of the office and smelled a crude odor. He visually inspected the station, and discovered a leak on the fill line at tank 26. The supervisor isolated the line. The section of the line that failed was visually examined by a corrosion subject matter expert, and determined to be internal corrosion. The line has been sent for lab analysis. An isolation valve was installed on the line. The line will be drained when not in use.
Report Received Date 2016-05-05 00:00:00
Iyear 2016
Report Number 20160139
Supplemental Number 21461
Report Type Supplemental Final
Operator Id 31957 PHMSA Enforcement
Name Kinder Morgan Wink Pipeline Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2016-04-06 09:35:00
Location Latitude 31.771673 Google Maps OpenStreetMap
Location Longitude -103.178171 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2016-04-06 09:35:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2016-04-06 09:35:00
Restart Datetime 2016-04-13 08:30:00
On Site Datetime 2016-04-06 09:35:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wink Station
Segment Name Tank 26 Fill Line
Onshore State Abbreviation Tx
Onshore Postal Code 79789
Onshore City Name Wink
Onshore County Name Winkler
Designated Location Milepost/valve Station
Designated Name 195
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.25
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Installation Year 1953
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 160
Est Cost Prop Damage 10000
Est Cost Emergency 0
Est Cost Environmental 13000
Est Cost Other 0
Prpty 23160
Accident Psig 16
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller is not able to see the tank fill line through scada, only the tank level. There were no scada indications of a leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Other Corrosion Ind Yes
Int Corrosion Type Details Scale Buildup - Under Deposit Corrosion
Int Field Exam Basis Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Failure Analysis And Microbial Assay
Int Other Loc Ind Yes
Corrosion Location Details Flange Entry Into Tank, Transition Between Pipe And Flange At 6 O'clock Position
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name A**** Z*****
Preparer Title Manager-Regulatory Compliance
Preparer Email A***********@k***********.com
Preparer Telephone 713-369-9512
Preparer Fax 303-984-3417
Prepared Date 2016-06-24 00:00:00
Authorizer Name S**** M*****
Authorizer Telephone 7133698065
Authorizer Title Director-Operations And Engineering
Authorizer Email S***********@k***********.com
Narrative On 4/6/2016, the wink station operations supervisor walked outside of the office and smelled a crude odor. He visually inspected the station, and discovered a leak on the fill line at tank 26. The supervisor isolated the line. The section of the line that failed was visually examined by a corrosion subject matter expert, and determined to be internal corrosion. The line has been sent for lab analysis. An isolation valve was installed on the line. The line will be drained when not in use.

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