GD incident on 2016-10-23 — MA

Operator
Boston Gas Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$33,538
Incident datetime
2016-10-23 23:07
Report number
Location
MA, SUFFOLK
Narrative
Cms dispatch was notified by revere police on 10/23 at 23:07 that a pipeline damage occurred. A cms crew was sent out and to investigate at 23:23 and cms dispatch was notified on 10/23 at 23:27 that a contractor installing a guardrail struck a 12" diameter, 100 psi natural gas distribution main. Main was shut down at 16:09 on 10/24 using a mechanical fitting. A 60 psi and a 25 psi regulator station were shutdown as well. Permanent repairs to 12" main were completed on 10/24 at 21:37. In total, 3000 hp and 591 lp customers were out of service (591 lp and 23 hp services were offline.) the last customer impacted by this outage was restored on 11/1/2016 at 11:30.
Detailed record list
Occurred At
2016-10-23 23:07:00
Year
2016
Report Received Date
2016-11-21 00:00:00
Iyear
2016.0
Report Number
20160120.0
Supplemental Number
16438.0
Report Type
Original Final
Operator Id
Name
Boston Gas Co
Operator Street Address
170 Data Drive
Operator City Name
Waltham
Operator State Abbreviation
MA
Operator Postal Code
02451
Local Datetime
2016-10-24 07:54:00
Location Street Address
Squire Rd And Route 1 North Side
Location City Name
Revere
Location County Name
Suffolk
Location State Abbreviation
MA
Location Postal Code
02151
Location Latitude
Location Longitude
Nrc Rpt Datetime
2016-10-25 15:34:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
4672.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2016-10-23 23:07:00
On Site Datetime
2016-10-23 23:23:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
32.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1952.0
Pipe Diameter
12.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.375
Release Type
Mechanical Puncture
Puncture Axial
2.3
Puncture Circum
2.5
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
33538.0
Est Cost Emergency
84786.0
Est Cost Other
0.0
Est Cost Unintentional Release
5716.0
Prpty
124040.0
Commercial Affected
20.0
Industrial Affected
0.0
Residences Affected
3571.0
Accident Psig
93.0
Normal Psig
95.0
Mop Psig
100.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Other
Accident Details
Local Police Called National Grid Call Center
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident was not caused by any actions of the control room or controller(s). It was a third party damage.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date
2016-01-01 00:00:00
Prior Notification Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
State Highway
Excavator Type
Contractor
Excavator Equipment
Unknown/other
Work Performed
Unknown/other
One Call Notified Ind
Yes
One Call Ticket Num
20164103937
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
16.0
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
C****** B*****
Preparer Title
Prin Prog Mgr Operations Codes And Policy
Preparer Email
C*************@n***********.com
Preparer Telephone
6317703549
Authorizer Name
C****** B*****
Authorizer Title
Principal Program Manager Federal Programs
Authorizer Telephone
6317703549
Authorizer Email
C*************@n***********.com
Narrative
Cms dispatch was notified by revere police on 10/23 at 23:07 that a pipeline damage occurred. A cms crew was sent out and to investigate at 23:23 and cms dispatch was notified on 10/23 at 23:27 that a contractor installing a guardrail struck a 12" diameter, 100 psi natural gas distribution main. Main was shut down at 16:09 on 10/24 using a mechanical fitting. A 60 psi and a 25 psi regulator station were shutdown as well. Permanent repairs to 12" main were completed on 10/24 at 21:37. In total, 3000 hp and 591 lp customers were out of service (591 lp and 23 hp services were offline.) the last customer impacted by this outage was restored on 11/1/2016 at 11:30.
Occurred At 2016-10-23 23:07:00
Year 2016
Report Received Date 2016-11-21 00:00:00
Iyear 2016.0
Report Number 20160120.0
Supplemental Number 16438.0
Report Type Original Final
Operator Id 1640 PHMSA Enforcement
Name Boston Gas Co
Operator Street Address 170 Data Drive
Operator City Name Waltham
Operator State Abbreviation MA
Operator Postal Code 02451
Local Datetime 2016-10-24 07:54:00
Location Street Address Squire Rd And Route 1 North Side
Location City Name Revere
Location County Name Suffolk
Location State Abbreviation MA
Location Postal Code 02151
Location Latitude 42.4275728 Google Maps OpenStreetMap
Location Longitude -71.0235477 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-10-25 15:34:00
Nrc Rpt Num 1162502 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 4672.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2016-10-23 23:07:00
On Site Datetime 2016-10-23 23:23:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 32.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1952.0
Pipe Diameter 12.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.375
Release Type Mechanical Puncture
Puncture Axial 2.3
Puncture Circum 2.5
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 33538.0
Est Cost Emergency 84786.0
Est Cost Other 0.0
Est Cost Unintentional Release 5716.0
Prpty 124040.0
Commercial Affected 20.0
Industrial Affected 0.0
Residences Affected 3571.0
Accident Psig 93.0
Normal Psig 95.0
Mop Psig 100.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Other
Accident Details Local Police Called National Grid Call Center
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident was not caused by any actions of the control room or controller(s). It was a third party damage.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date 2016-01-01 00:00:00
Prior Notification Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype State Highway
Excavator Type Contractor
Excavator Equipment Unknown/other
Work Performed Unknown/other
One Call Notified Ind Yes
One Call Ticket Num 20164103937
Locator Type Contract Locator
Visible Marks No
Service Interruption Yes
Service Interruption Hours 16.0
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name C****** B*****
Preparer Title Prin Prog Mgr Operations Codes And Policy
Preparer Email C*************@n***********.com
Preparer Telephone 6317703549
Authorizer Name C****** B*****
Authorizer Title Principal Program Manager Federal Programs
Authorizer Telephone 6317703549
Authorizer Email C*************@n***********.com
Narrative Cms dispatch was notified by revere police on 10/23 at 23:07 that a pipeline damage occurred. A cms crew was sent out and to investigate at 23:23 and cms dispatch was notified on 10/23 at 23:27 that a contractor installing a guardrail struck a 12" diameter, 100 psi natural gas distribution main. Main was shut down at 16:09 on 10/24 using a mechanical fitting. A 60 psi and a 25 psi regulator station were shutdown as well. Permanent repairs to 12" main were completed on 10/24 at 21:37. In total, 3000 hp and 591 lp customers were out of service (591 lp and 23 hp services were offline.) the last customer impacted by this outage was restored on 11/1/2016 at 11:30.

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