GD incident on 2016-08-31 — KS

Operator
Atmos Energy Corporation - Colorado/kansas
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2016-08-31 12:15
Report number
Location
KS, HAMILTON
Narrative
Farmer damaged main with a root cutting implement in a remote area where water runoff caused main to become shallow. The farmer was not aware of the damage, therefore did not report to the utility. Several days later, company crews were in process of repairing a leak on the same line when the pressure was discovered to be lower than normal, but higher than the low alarm limit of the remote pressure monitors. The operator personnel then began investigating and found the location of the damage. Valves were utilized to shut down a short section of main being fed from 2 directions, which allowed the damage to be repaired.
Detailed record list
Occurred At
2016-08-31 12:15:00
Year
2016
Report Received Date
2016-09-26 00:00:00
Iyear
2016.0
Report Number
20160096.0
Supplemental Number
16519.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Colorado/kansas
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2016-08-20 12:30:00
Location Street Address
Approximate Intersection Of Road 30 And Road I
Location City Name
Not Within A Municipality
Location County Name
Hamilton
Location State Abbreviation
KS
Location Postal Code
67878
Location Latitude
Location Longitude
-101.8998325
Nrc Rpt Datetime
2016-09-09 14:51:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
45420.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2016-08-31 12:15:00
On Site Datetime
2016-08-31 12:15:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
3.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Pipe Diameter
4.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Mechanical Puncture
Puncture Axial
0.6
Puncture Circum
1.3
Class Location Type
Class 1 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
5000.0
Est Cost Emergency
1000.0
Est Cost Other
0.0
Est Cost Unintentional Release
136260.0
Prpty
142260.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
218.0
Normal Psig
257.0
Mop Psig
285.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pressure monitoring point did not reach the low alarm limit
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Excavator Type
Farmer
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
No
Service Interruption
No
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
No One-Call Notification Coupled With Shallow Main
Preparer Name
D****** S*****
Preparer Title
Compliance Manager
Preparer Email
D**********@a**********.com
Preparer Telephone
8168630951
Authorizer Name
D****** S*****
Authorizer Title
Manager Of Compliance
Authorizer Telephone
816-863-0951
Authorizer Email
D**********@a**********.com
Narrative
Farmer damaged main with a root cutting implement in a remote area where water runoff caused main to become shallow. The farmer was not aware of the damage, therefore did not report to the utility. Several days later, company crews were in process of repairing a leak on the same line when the pressure was discovered to be lower than normal, but higher than the low alarm limit of the remote pressure monitors. The operator personnel then began investigating and found the location of the damage. Valves were utilized to shut down a short section of main being fed from 2 directions, which allowed the damage to be repaired.
Occurred At 2016-08-31 12:15:00
Year 2016
Report Received Date 2016-09-26 00:00:00
Iyear 2016.0
Report Number 20160096.0
Supplemental Number 16519.0
Report Type Supplemental Final
Operator Id 6720 PHMSA Enforcement
Name Atmos Energy Corporation - Colorado/kansas
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2016-08-20 12:30:00
Location Street Address Approximate Intersection Of Road 30 And Road I
Location City Name Not Within A Municipality
Location County Name Hamilton
Location State Abbreviation KS
Location Postal Code 67878
Location Latitude 37.85146 Google Maps OpenStreetMap
Location Longitude -101.8998325 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-09-09 14:51:00
Nrc Rpt Num 1158594 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 45420.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2016-08-31 12:15:00
On Site Datetime 2016-08-31 12:15:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 3.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Pipe Diameter 4.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Mechanical Puncture
Puncture Axial 0.6
Puncture Circum 1.3
Class Location Type Class 1 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 5000.0
Est Cost Emergency 1000.0
Est Cost Other 0.0
Est Cost Unintentional Release 136260.0
Prpty 142260.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 218.0
Normal Psig 257.0
Mop Psig 285.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pressure monitoring point did not reach the low alarm limit
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Excavator Type Farmer
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind No
Service Interruption No
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other No One-Call Notification Coupled With Shallow Main
Preparer Name D****** S*****
Preparer Title Compliance Manager
Preparer Email D**********@a**********.com
Preparer Telephone 8168630951
Authorizer Name D****** S*****
Authorizer Title Manager Of Compliance
Authorizer Telephone 816-863-0951
Authorizer Email D**********@a**********.com
Narrative Farmer damaged main with a root cutting implement in a remote area where water runoff caused main to become shallow. The farmer was not aware of the damage, therefore did not report to the utility. Several days later, company crews were in process of repairing a leak on the same line when the pressure was discovered to be lower than normal, but higher than the low alarm limit of the remote pressure monitors. The operator personnel then began investigating and found the location of the damage. Valves were utilized to shut down a short section of main being fed from 2 directions, which allowed the damage to be repaired.

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