GD incident on 2016-08-10 — OK

Operator
City Of Hooker
Cause
Other Incident Cause
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2016-08-10 09:06
Report number
Location
OK, TEXAS
Narrative

No narrative available.

Detailed record list
Occurred At
2016-08-10 09:06:00
Year
2016
Report Received Date
2016-09-08 00:00:00
Iyear
2016.0
Report Number
20160083.0
Supplemental Number
16379.0
Report Type
Original
Operator Id
Name
City Of Hooker
Operator Street Address
111 S Broadways
Operator City Name
Hooker
Operator State Abbreviation
OK
Operator Postal Code
73945
Local Datetime
2016-08-10 09:06:00
Location Street Address
300 Blk W. Clarence Street/ Us Hwy 54
Location City Name
Hooker
Location County Name
Texas
Location State Abbreviation
OK
Location Postal Code
73945
Location Latitude
Location Longitude
Nrc Rpt Datetime
2016-08-10 16:00:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
140.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2016-08-10 09:06:00
On Site Datetime
2016-08-10 09:06:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
63.0
Crossing
No
Pipe Facility Type
Municipally Owned
System Part Involved
Main
Installation Year
1975.0
Pipe Diameter
4.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Steel Seam Type Details
Seamless
Wt Steel
1.237
Release Type
Other
Release Type Details
A 2 In Poly By-Pass Line Was Burned Secondary From An Primary Fire In A Demolition Activity
Class Location Type
Class 3 Location
Est Cost Oper Paid
42000.0
Est Cost Prop Damage
0.0
Est Cost Emergency
0.0
Est Cost Other
26000.0
Est Cost Other Details
Treatment And Emergency Transport To Employee
Est Cost Unintentional Release
58.0
Prpty
68058.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
60.0
Normal Psig
60.0
Mop Psig
200.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
6
Num Contractors Failed
0
Cause
Other Incident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
During Removal Of A Vessel A Minor Fire Ignited Resulted From Residue In The Pipe Which Melted A 2 In Poly By-Pass To Supply The Distribution System.
Preparer Name
R****** E* H******
Preparer Title
Superindenant
Preparer Email
P**********@h*************.net
Preparer Telephone
580-652-2885
Preparer Fax
580-652-2488
Authorizer Name
R****** E* H******
Authorizer Title
Superentident
Authorizer Telephone
580-652-2885
Authorizer Email
P**********@h*************.net
Occurred At 2016-08-10 09:06:00
Year 2016
Report Received Date 2016-09-08 00:00:00
Iyear 2016.0
Report Number 20160083.0
Supplemental Number 16379.0
Report Type Original
Operator Id 31597 PHMSA Enforcement
Name City Of Hooker
Operator Street Address 111 S Broadways
Operator City Name Hooker
Operator State Abbreviation OK
Operator Postal Code 73945
Local Datetime 2016-08-10 09:06:00
Location Street Address 300 Blk W. Clarence Street/ Us Hwy 54
Location City Name Hooker
Location County Name Texas
Location State Abbreviation OK
Location Postal Code 73945
Location Latitude 36.855325 Google Maps OpenStreetMap
Location Longitude -101.214839 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-08-10 16:00:00
Nrc Rpt Num 1155868 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 140.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2016-08-10 09:06:00
On Site Datetime 2016-08-10 09:06:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 63.0
Crossing No
Pipe Facility Type Municipally Owned
System Part Involved Main
Installation Year 1975.0
Pipe Diameter 4.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Steel Seam Type Details Seamless
Wt Steel 1.237
Release Type Other
Release Type Details A 2 In Poly By-Pass Line Was Burned Secondary From An Primary Fire In A Demolition Activity
Class Location Type Class 3 Location
Est Cost Oper Paid 42000.0
Est Cost Prop Damage 0.0
Est Cost Emergency 0.0
Est Cost Other 26000.0
Est Cost Other Details Treatment And Emergency Transport To Employee
Est Cost Unintentional Release 58.0
Prpty 68058.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 60.0
Normal Psig 60.0
Mop Psig 200.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 6
Num Contractors Failed 0
Cause Other Incident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details During Removal Of A Vessel A Minor Fire Ignited Resulted From Residue In The Pipe Which Melted A 2 In Poly By-Pass To Supply The Distribution System.
Preparer Name R****** E* H******
Preparer Title Superindenant
Preparer Email P**********@h*************.net
Preparer Telephone 580-652-2885
Preparer Fax 580-652-2488
Authorizer Name R****** E* H******
Authorizer Title Superentident
Authorizer Telephone 580-652-2885
Authorizer Email P**********@h*************.net

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