GD incident on 2016-08-09 — NJ

Operator
New Jersey Natural Gas Co
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$0
Incident datetime
2016-08-09 13:42
Report number
Location
NJ, MONMOUTH
Narrative
The incident occurred at the site of a corroded service tee. This service had been classified as a bare steel service. Njng has a program to comply with state regulations where bare steel service in a defined area is replace if 20% or more of bare steel services are exhibiting leaks. During this replacement work contractor crew discovered the leak and notified the gas company. Our company crew arrived on site and proceeded to repair/retire the service tee. During the repair process, the crew mechanic utilized a tool to remove the damaged service tee that is not recommended for use in a gaseous environment, this tool may have been the cause of ignition. The crew mechanic was admitted to the hospital with burns to his arms. In its interviews with the injured employee and his crew leader, njng has learned the responding employees failed to follow the guidelines for wearing proper fire protection attire before entry into a gaseous environment, including failure to use breathing apparatus. Both responding employees were fully trained and qualified in conformance with our operator qualification ('oq') program at the time of the incident. In addition, the company provides safety training beyond oq including fire safety, burn prevention, personal protective equipment and respiratory protection and fit testing. Post-incident, njng's manager training & field support disqualified both responding employees from oq task #39 ' remove service tee or fitting from steel and cast iron mains. Therefore, the responding employees will not perform these tasks until they are retrained/requalified.
Detailed record list
Occurred At
2016-08-09 13:42:00
Year
2016
Report Received Date
2016-09-07 00:00:00
Iyear
2016.0
Report Number
20160081.0
Supplemental Number
16790.0
Report Type
Supplemental Final
Operator Id
Name
New Jersey Natural Gas Co
Operator Street Address
1415 Wyckoff Road
Operator City Name
Wall
Operator State Abbreviation
NJ
Operator Postal Code
07719
Local Datetime
2016-08-09 13:42:00
Location Street Address
271 Harmony Rd
Location City Name
Middletown
Location County Name
Monmouth
Location State Abbreviation
NJ
Location Postal Code
07748
Location Latitude
Location Longitude
Nrc Rpt Datetime
2016-08-09 17:13:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
0.01
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2016-08-09 13:42:00
On Site Datetime
2016-08-09 13:42:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
44.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service
Installation Year
1957.0
Pipe Diameter
4.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.237
Release Type
Leak
Leak Type
Other
Leak Type Other
Corrosion
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
0.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
10.0
Prpty
10.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
35.0
Normal Psig
35.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
Yes
Num Employees Tested
5
Num Employees Failed
0
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Improper Equipment Was Used To Cut Off The Service Tee.
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
M***** K***
Preparer Title
Director
Preparer Email
M*****@n***.com
Preparer Telephone
732 919 8035
Preparer Fax
732 919 0936
Authorizer Name
M***** K***
Authorizer Title
Director
Authorizer Telephone
732 919 8035
Authorizer Email
M*****@n***.com
Narrative
The incident occurred at the site of a corroded service tee. This service had been classified as a bare steel service. Njng has a program to comply with state regulations where bare steel service in a defined area is replace if 20% or more of bare steel services are exhibiting leaks. During this replacement work contractor crew discovered the leak and notified the gas company. Our company crew arrived on site and proceeded to repair/retire the service tee. During the repair process, the crew mechanic utilized a tool to remove the damaged service tee that is not recommended for use in a gaseous environment, this tool may have been the cause of ignition. The crew mechanic was admitted to the hospital with burns to his arms. In its interviews with the injured employee and his crew leader, njng has learned the responding employees failed to follow the guidelines for wearing proper fire protection attire before entry into a gaseous environment, including failure to use breathing apparatus. Both responding employees were fully trained and qualified in conformance with our operator qualification ('oq') program at the time of the incident. In addition, the company provides safety training beyond oq including fire safety, burn prevention, personal protective equipment and respiratory protection and fit testing. Post-incident, njng's manager training & field support disqualified both responding employees from oq task #39 ' remove service tee or fitting from steel and cast iron mains. Therefore, the responding employees will not perform these tasks until they are retrained/requalified.
Occurred At 2016-08-09 13:42:00
Year 2016
Report Received Date 2016-09-07 00:00:00
Iyear 2016.0
Report Number 20160081.0
Supplemental Number 16790.0
Report Type Supplemental Final
Operator Id 13299 PHMSA Enforcement
Name New Jersey Natural Gas Co
Operator Street Address 1415 Wyckoff Road
Operator City Name Wall
Operator State Abbreviation NJ
Operator Postal Code 07719
Local Datetime 2016-08-09 13:42:00
Location Street Address 271 Harmony Rd
Location City Name Middletown
Location County Name Monmouth
Location State Abbreviation NJ
Location Postal Code 07748
Location Latitude 40.416981 Google Maps OpenStreetMap
Location Longitude -74.123134 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-08-09 17:13:00
Nrc Rpt Num 1155755 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 0.01
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2016-08-09 13:42:00
On Site Datetime 2016-08-09 13:42:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 44.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service
Installation Year 1957.0
Pipe Diameter 4.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.237
Release Type Leak
Leak Type Other
Leak Type Other Corrosion
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 0.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 10.0
Prpty 10.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 35.0
Normal Psig 35.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind Yes
Num Employees Tested 5
Num Employees Failed 0
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Improper Equipment Was Used To Cut Off The Service Tee.
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name M***** K***
Preparer Title Director
Preparer Email M*****@n***.com
Preparer Telephone 732 919 8035
Preparer Fax 732 919 0936
Authorizer Name M***** K***
Authorizer Title Director
Authorizer Telephone 732 919 8035
Authorizer Email M*****@n***.com
Narrative The incident occurred at the site of a corroded service tee. This service had been classified as a bare steel service. Njng has a program to comply with state regulations where bare steel service in a defined area is replace if 20% or more of bare steel services are exhibiting leaks. During this replacement work contractor crew discovered the leak and notified the gas company. Our company crew arrived on site and proceeded to repair/retire the service tee. During the repair process, the crew mechanic utilized a tool to remove the damaged service tee that is not recommended for use in a gaseous environment, this tool may have been the cause of ignition. The crew mechanic was admitted to the hospital with burns to his arms. In its interviews with the injured employee and his crew leader, njng has learned the responding employees failed to follow the guidelines for wearing proper fire protection attire before entry into a gaseous environment, including failure to use breathing apparatus. Both responding employees were fully trained and qualified in conformance with our operator qualification ('oq') program at the time of the incident. In addition, the company provides safety training beyond oq including fire safety, burn prevention, personal protective equipment and respiratory protection and fit testing. Post-incident, njng's manager training & field support disqualified both responding employees from oq task #39 ' remove service tee or fitting from steel and cast iron mains. Therefore, the responding employees will not perform these tasks until they are retrained/requalified.

All rights reserved. Copyright © by ClearPHMSA