GD incident on 2016-08-08 — MA

Operator
Boston Gas Co
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2016-08-08 10:50
Report number
Location
MA, ESSEX
Narrative
At 10:32 on 8/8/2016, an emergency response unit was dispatched to 107 low st following a reported hit line by a 3rd party contractor, granese construction. One-call was notified but maps/records were not available. Between 12:30 and 13:30, preparations were made to shutdown the main and associated services. Three customers were evacuated; a total of 35 customers were out of service. Main and services were isolated using system isolation valves, completed by 17:00. At 22:20, mueller stop-off fitting was installed temporarily to secure leak and additional repairs were made to main. Approx. An 8 foot section of main was replaced. Repairs were completed by 3:48 on 8/9/2016, and at 4:20, gas was reintroduced to main and valves reopened. At 6:00, relights were started.There currently are 3 "cannot get in" customers with cards left to notify them to schedule relights.
Detailed record list
Occurred At
2016-08-08 10:50:00
Year
2016
Report Received Date
2016-09-04 00:00:00
Iyear
2016.0
Report Number
20160079.0
Supplemental Number
16374.0
Report Type
Original Final
Operator Id
Name
Boston Gas Co
Operator Street Address
170 Data Drive
Operator City Name
Waltham
Operator State Abbreviation
MA
Operator Postal Code
02451
Local Datetime
2016-08-08 10:32:00
Location Street Address
107 Low Street
Location City Name
Newburyport
Location County Name
Essex
Location State Abbreviation
MA
Location Postal Code
01950
Location Latitude
Location Longitude
Nrc Rpt Datetime
2016-08-11 16:57:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
3824.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
3.0
Incident Identified Datetime
2016-08-08 10:50:00
On Site Datetime
2016-08-08 10:56:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1982.0
Pipe Diameter
10.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Mechanical Puncture
Puncture Axial
0.3
Puncture Circum
13.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
2500.0
Est Cost Emergency
15000.0
Est Cost Other
0.0
Est Cost Unintentional Release
5500.0
Prpty
23000.0
Commercial Affected
30.0
Industrial Affected
0.0
Residences Affected
5.0
Accident Psig
55.03
Normal Psig
55.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident was due to third party damage, and was confirmed by first responder.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date
2015-01-01 00:00:00
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Trencher
Work Performed
Drainage
One Call Notified Ind
Yes
One Call Ticket Num
20162900357
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
12.0
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Data Not Collected
Preparer Name
C****** B*****
Preparer Title
Principal Program Manager Federal Programs
Preparer Email
C*************@n***********.com
Preparer Telephone
6317703549
Authorizer Name
C****** B*****
Authorizer Title
Principal Program Manager Federal Program
Authorizer Telephone
6317703549
Authorizer Email
C*************@n***********.com
Narrative
At 10:32 on 8/8/2016, an emergency response unit was dispatched to 107 low st following a reported hit line by a 3rd party contractor, granese construction. One-call was notified but maps/records were not available. Between 12:30 and 13:30, preparations were made to shutdown the main and associated services. Three customers were evacuated; a total of 35 customers were out of service. Main and services were isolated using system isolation valves, completed by 17:00. At 22:20, mueller stop-off fitting was installed temporarily to secure leak and additional repairs were made to main. Approx. An 8 foot section of main was replaced. Repairs were completed by 3:48 on 8/9/2016, and at 4:20, gas was reintroduced to main and valves reopened. At 6:00, relights were started.There currently are 3 "cannot get in" customers with cards left to notify them to schedule relights.
Occurred At 2016-08-08 10:50:00
Year 2016
Report Received Date 2016-09-04 00:00:00
Iyear 2016.0
Report Number 20160079.0
Supplemental Number 16374.0
Report Type Original Final
Operator Id 1640 PHMSA Enforcement
Name Boston Gas Co
Operator Street Address 170 Data Drive
Operator City Name Waltham
Operator State Abbreviation MA
Operator Postal Code 02451
Local Datetime 2016-08-08 10:32:00
Location Street Address 107 Low Street
Location City Name Newburyport
Location County Name Essex
Location State Abbreviation MA
Location Postal Code 01950
Location Latitude 42.808176 Google Maps OpenStreetMap
Location Longitude -70.889677 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-08-11 16:57:00
Nrc Rpt Num 1155977 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 3824.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 3.0
Incident Identified Datetime 2016-08-08 10:50:00
On Site Datetime 2016-08-08 10:56:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1982.0
Pipe Diameter 10.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Mechanical Puncture
Puncture Axial 0.3
Puncture Circum 13.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 2500.0
Est Cost Emergency 15000.0
Est Cost Other 0.0
Est Cost Unintentional Release 5500.0
Prpty 23000.0
Commercial Affected 30.0
Industrial Affected 0.0
Residences Affected 5.0
Accident Psig 55.03
Normal Psig 55.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident was due to third party damage, and was confirmed by first responder.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date 2015-01-01 00:00:00
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Trencher
Work Performed Drainage
One Call Notified Ind Yes
One Call Ticket Num 20162900357
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 12.0
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Data Not Collected
Preparer Name C****** B*****
Preparer Title Principal Program Manager Federal Programs
Preparer Email C*************@n***********.com
Preparer Telephone 6317703549
Authorizer Name C****** B*****
Authorizer Title Principal Program Manager Federal Program
Authorizer Telephone 6317703549
Authorizer Email C*************@n***********.com
Narrative At 10:32 on 8/8/2016, an emergency response unit was dispatched to 107 low st following a reported hit line by a 3rd party contractor, granese construction. One-call was notified but maps/records were not available. Between 12:30 and 13:30, preparations were made to shutdown the main and associated services. Three customers were evacuated; a total of 35 customers were out of service. Main and services were isolated using system isolation valves, completed by 17:00. At 22:20, mueller stop-off fitting was installed temporarily to secure leak and additional repairs were made to main. Approx. An 8 foot section of main was replaced. Repairs were completed by 3:48 on 8/9/2016, and at 4:20, gas was reintroduced to main and valves reopened. At 6:00, relights were started.There currently are 3 "cannot get in" customers with cards left to notify them to schedule relights.

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