GD incident on 2016-03-21 — OH

Operator
Duke Energy Ohio
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,250
Incident datetime
2016-03-21 10:27
Report number
Location
OH, BUTLER
Narrative
Duke energy's investigation revealed a couple of factors contributed to the cause of the incident. First, the contractor hired by duke energy (usic locating services, inc.) to locate the facilities did not follow the procedure when dealing with an untoneable service. Duke energy has a procedure that requires the locating company to take additional steps when locating untoneable services. Second, the plumber performing the work used a track hoe to excavate inside the tolerance zone instead of hand digging to locate the service.
Detailed record list
Occurred At
2016-03-21 10:27:00
Year
2016
Report Received Date
2016-04-19 00:00:00
Iyear
2016.0
Report Number
20160038.0
Supplemental Number
16303.0
Report Type
Supplemental Final
Operator Id
Name
Duke Energy Ohio
Operator Street Address
139 East Fourth Street Po Box 960 - Room 460-Annex
Operator City Name
Cincinnati
Operator State Abbreviation
OH
Operator Postal Code
45202
Local Datetime
2016-03-21 10:22:00
Location Street Address
46 Woodstock Drive
Location City Name
Fairfield
Location County Name
Butler
Location State Abbreviation
OH
Location Postal Code
45014
Location Latitude
Location Longitude
Nrc Rpt Datetime
2016-03-21 11:28:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
1274.26
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
20.0
Incident Identified Datetime
2016-03-21 10:27:00
On Site Datetime
2016-03-21 10:41:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24.0
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service
Installation Year
1973.0
Pipe Diameter
1.25
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Wt Plastic Unknown Ind
Unknown
Material Pe Pipe Code
Unknown
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
0.5
Class Location Type
Class 4 Location
Est Cost Oper Paid
600000.0
Est Cost Prop Damage
10250.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
0.0
Prpty
610250.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
20.0
Accident Psig
41.0
Normal Psig
41.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a third party damage
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date
2014-01-01 00:00:00
Ex Hydrotest Conducted Ind
No
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Easement
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
607601201
One Call Center Name
Ohio Utilities Protection Service
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
8.0
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Locating And Excavation Practices Not Sufficient.
Preparer Name
R**** S******
Preparer Title
Senior Regulatory Compliance Specialist
Preparer Email
R**************@d**********.com
Preparer Telephone
513-287-3346
Authorizer Name
C******* T*****
Authorizer Title
Manager Gas Compliance
Authorizer Telephone
513-287-3781
Authorizer Email
C**************@d**********.com
Narrative
Duke energy's investigation revealed a couple of factors contributed to the cause of the incident. First, the contractor hired by duke energy (usic locating services, inc.) to locate the facilities did not follow the procedure when dealing with an untoneable service. Duke energy has a procedure that requires the locating company to take additional steps when locating untoneable services. Second, the plumber performing the work used a track hoe to excavate inside the tolerance zone instead of hand digging to locate the service.
Occurred At 2016-03-21 10:27:00
Year 2016
Report Received Date 2016-04-19 00:00:00
Iyear 2016.0
Report Number 20160038.0
Supplemental Number 16303.0
Report Type Supplemental Final
Operator Id 2364 PHMSA Enforcement
Name Duke Energy Ohio
Operator Street Address 139 East Fourth Street Po Box 960 - Room 460-Annex
Operator City Name Cincinnati
Operator State Abbreviation OH
Operator Postal Code 45202
Local Datetime 2016-03-21 10:22:00
Location Street Address 46 Woodstock Drive
Location City Name Fairfield
Location County Name Butler
Location State Abbreviation OH
Location Postal Code 45014
Location Latitude 39.317028 Google Maps OpenStreetMap
Location Longitude -84.505248 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-03-21 11:28:00
Nrc Rpt Num 1143355 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1274.26
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 20.0
Incident Identified Datetime 2016-03-21 10:27:00
On Site Datetime 2016-03-21 10:41:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24.0
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Service
Installation Year 1973.0
Pipe Diameter 1.25
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Wt Plastic Unknown Ind Unknown
Material Pe Pipe Code Unknown
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 0.5
Class Location Type Class 4 Location
Est Cost Oper Paid 600000.0
Est Cost Prop Damage 10250.0
Est Cost Emergency 0.0
Est Cost Other 0.0
Est Cost Unintentional Release 0.0
Prpty 610250.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 20.0
Accident Psig 41.0
Normal Psig 41.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a third party damage
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Ex Hydrotest Leak Survey Date 2014-01-01 00:00:00
Ex Hydrotest Conducted Ind No
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Easement
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num 607601201
One Call Center Name Ohio Utilities Protection Service
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 8.0
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Locating And Excavation Practices Not Sufficient.
Preparer Name R**** S******
Preparer Title Senior Regulatory Compliance Specialist
Preparer Email R**************@d**********.com
Preparer Telephone 513-287-3346
Authorizer Name C******* T*****
Authorizer Title Manager Gas Compliance
Authorizer Telephone 513-287-3781
Authorizer Email C**************@d**********.com
Narrative Duke energy's investigation revealed a couple of factors contributed to the cause of the incident. First, the contractor hired by duke energy (usic locating services, inc.) to locate the facilities did not follow the procedure when dealing with an untoneable service. Duke energy has a procedure that requires the locating company to take additional steps when locating untoneable services. Second, the plumber performing the work used a track hoe to excavate inside the tolerance zone instead of hand digging to locate the service.

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