GD incident on 2016-02-24 — MO

Operator
Laclede Gas Co
Cause
Pipe, Weld, Or Joint Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$114,000
Incident datetime
2016-02-24 08:20
Report number
Location
MO, SAINT LOUIS
Narrative
After completing a leak investigation from a customer reported call of a slight inside odor, it was determined a nearby 24 inch cast iron main was leaking. Excavation crews had difficulty reaching the main due its depth of 84 inches along with the concrete and brick found below the pipe. Two longitudinal cracks totaling 32 inches in length were found on the bottom section of the pipe. Installation of a stainless steel clamp was attempted to repair the leak; however it was unsuccessful. The incident was deemed to be reportable on february 27, 2016, when it was determined that the repair costs would probably exceed $50,000. The company ordered a 44 inch long steel, split sleeve encapsulation fitting as an alternate repair. The encapsulation fitting required additional excavation of the pipe which uncovered a third crack 16 inches long. The encapsulation fitting was successfully installed around the original two cracks. The third crack was soap taped as a temporary repair. Service technicians remained onsite to monitor the leak while the repairs were made. It is unclear if the pipe was constructed resting on concrete and brick or if subsidence over the past 113 years moved the pipe to its current position. The company is also unable to determine if outside forces from the traffic above the pipe was a contributing factor to the failure. The uncertainty of the root cause of failure has prompted the company to accelerate its plans for full replacement of this pipe segment and adjoining main. The company has proposed replacing or abandoning approximately 2,800 feet of the 24 inch cast iron main involved and approximately 900 feet of 12 inch cast iron main.
Detailed record list
Occurred At
2016-02-24 08:20:00
Year
2016
Report Received Date
2016-03-25 00:00:00
Iyear
2016.0
Report Number
20160029.0
Supplemental Number
16338.0
Report Type
Supplemental Final
Operator Id
Name
Laclede Gas Co
Operator Street Address
700 Market Street
Operator City Name
Saint Louis
Operator State Abbreviation
MO
Operator Postal Code
63101
Local Datetime
2016-02-24 07:52:00
Location Street Address
1010 Saint Charles St
Location City Name
Saint Louis
Location County Name
Saint Louis
Location State Abbreviation
MO
Location Postal Code
63101
Location Latitude
Location Longitude
Nrc Rpt Datetime
2016-02-27 09:45:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
1420.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2016-02-24 08:20:00
On Site Datetime
2016-02-24 08:43:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
84.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1903.0
Pipe Diameter
24.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Cast/wrought Iron
Release Type
Leak
Leak Type
Crack
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
114000.0
Est Cost Emergency
500.0
Est Cost Other
0.0
Est Cost Unintentional Release
6093.0
Prpty
120593.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
12.0
Normal Psig
12.0
Mop Psig
25.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind
Yes
Invest No Schedule Ind Details
System Pressure Was Not A Contributing Factor To The Leak
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Pipe, Weld, Or Joint Failure
Cause Details
Body Of Pipe
Pwjf Failure Type
Body Of Pipe
Pipe Body Subtype
Crack
Additional Crack Ind
Yes
Additional Other Ind
Yes
Additional Factor Details
Outside Forces From The Traffic Above The Pipe And Subsidance Near Concrete And Brick May Have Been Contributing Factors To The Failure.
Result Material Ind
Yes
Result Material Subtype
Other
Result Material Details
Cast Iron
Hydrotest Conducted Ind
No
Preparer Name
P****** S*******
Preparer Title
Manager Of Pipeline Safety And Compliance
Preparer Email
P***************@t**************.com
Preparer Telephone
(314) 349-2936
Authorizer Name
C**** R* H********
Authorizer Title
Vice President Of Operations Services
Authorizer Telephone
(314) 349-2972
Authorizer Email
C**************@t**************.com
Narrative
After completing a leak investigation from a customer reported call of a slight inside odor, it was determined a nearby 24 inch cast iron main was leaking. Excavation crews had difficulty reaching the main due its depth of 84 inches along with the concrete and brick found below the pipe. Two longitudinal cracks totaling 32 inches in length were found on the bottom section of the pipe. Installation of a stainless steel clamp was attempted to repair the leak; however it was unsuccessful. The incident was deemed to be reportable on february 27, 2016, when it was determined that the repair costs would probably exceed $50,000. The company ordered a 44 inch long steel, split sleeve encapsulation fitting as an alternate repair. The encapsulation fitting required additional excavation of the pipe which uncovered a third crack 16 inches long. The encapsulation fitting was successfully installed around the original two cracks. The third crack was soap taped as a temporary repair. Service technicians remained onsite to monitor the leak while the repairs were made. It is unclear if the pipe was constructed resting on concrete and brick or if subsidence over the past 113 years moved the pipe to its current position. The company is also unable to determine if outside forces from the traffic above the pipe was a contributing factor to the failure. The uncertainty of the root cause of failure has prompted the company to accelerate its plans for full replacement of this pipe segment and adjoining main. The company has proposed replacing or abandoning approximately 2,800 feet of the 24 inch cast iron main involved and approximately 900 feet of 12 inch cast iron main.
Occurred At 2016-02-24 08:20:00
Year 2016
Report Received Date 2016-03-25 00:00:00
Iyear 2016.0
Report Number 20160029.0
Supplemental Number 16338.0
Report Type Supplemental Final
Operator Id 11032 PHMSA Enforcement
Name Laclede Gas Co
Operator Street Address 700 Market Street
Operator City Name Saint Louis
Operator State Abbreviation MO
Operator Postal Code 63101
Local Datetime 2016-02-24 07:52:00
Location Street Address 1010 Saint Charles St
Location City Name Saint Louis
Location County Name Saint Louis
Location State Abbreviation MO
Location Postal Code 63101
Location Latitude 38.629945 Google Maps OpenStreetMap
Location Longitude -90.194248 Google Maps OpenStreetMap
Nrc Rpt Datetime 2016-02-27 09:45:00
Nrc Rpt Num 1141503 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1420.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2016-02-24 08:20:00
On Site Datetime 2016-02-24 08:43:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 84.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1903.0
Pipe Diameter 24.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Cast/wrought Iron
Release Type Leak
Leak Type Crack
Class Location Type Class 4 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 114000.0
Est Cost Emergency 500.0
Est Cost Other 0.0
Est Cost Unintentional Release 6093.0
Prpty 120593.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 12.0
Normal Psig 12.0
Mop Psig 25.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Schedule Ind Yes
Invest No Schedule Ind Details System Pressure Was Not A Contributing Factor To The Leak
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Pipe, Weld, Or Joint Failure
Cause Details Body Of Pipe
Pwjf Failure Type Body Of Pipe
Pipe Body Subtype Crack
Additional Crack Ind Yes
Additional Other Ind Yes
Additional Factor Details Outside Forces From The Traffic Above The Pipe And Subsidance Near Concrete And Brick May Have Been Contributing Factors To The Failure.
Result Material Ind Yes
Result Material Subtype Other
Result Material Details Cast Iron
Hydrotest Conducted Ind No
Preparer Name P****** S*******
Preparer Title Manager Of Pipeline Safety And Compliance
Preparer Email P***************@t**************.com
Preparer Telephone (314) 349-2936
Authorizer Name C**** R* H********
Authorizer Title Vice President Of Operations Services
Authorizer Telephone (314) 349-2972
Authorizer Email C**************@t**************.com
Narrative After completing a leak investigation from a customer reported call of a slight inside odor, it was determined a nearby 24 inch cast iron main was leaking. Excavation crews had difficulty reaching the main due its depth of 84 inches along with the concrete and brick found below the pipe. Two longitudinal cracks totaling 32 inches in length were found on the bottom section of the pipe. Installation of a stainless steel clamp was attempted to repair the leak; however it was unsuccessful. The incident was deemed to be reportable on february 27, 2016, when it was determined that the repair costs would probably exceed $50,000. The company ordered a 44 inch long steel, split sleeve encapsulation fitting as an alternate repair. The encapsulation fitting required additional excavation of the pipe which uncovered a third crack 16 inches long. The encapsulation fitting was successfully installed around the original two cracks. The third crack was soap taped as a temporary repair. Service technicians remained onsite to monitor the leak while the repairs were made. It is unclear if the pipe was constructed resting on concrete and brick or if subsidence over the past 113 years moved the pipe to its current position. The company is also unable to determine if outside forces from the traffic above the pipe was a contributing factor to the failure. The uncertainty of the root cause of failure has prompted the company to accelerate its plans for full replacement of this pipe segment and adjoining main. The company has proposed replacing or abandoning approximately 2,800 feet of the 24 inch cast iron main involved and approximately 900 feet of 12 inch cast iron main.

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