Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2015-02-11 — NY
Operator
Keyspan Energy Delivery - Long Island
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
2 injuries
Property damage (nominal)
$0
Incident datetime
2015-02-11 14:28
Report number
Location
NY, SUFFOLK
Narrative
Based on the preliminary investigation it appears the gas leak on piping located in the basement of the premises, renovation work was ongoing and the workers reported to the police that they had cut through internal piping immediately prior to the incident. The company conducted a pressure test on the gas service line to the premises following the incident; no leaks were detected on the service line. There is no relevant leak history in the area or other indication of issues with the company's gas facilities. The account was inactive at the time of the incident
Detailed record list
Occurred At
2015-02-11 14:28:00
Year
2015
Report Received Date
2016-02-19 00:00:00
Iyear
2015.0
Report Number
20160016.0
Supplemental Number
16608.0
Report Type
Supplemental Final
Operator Id
11713
Name
Keyspan Energy Delivery - Long Island
Operator Street Address
175 East Old Country Road
Operator City Name
Hicksville
Operator State Abbreviation
NY
Operator Postal Code
11801
Local Datetime
2015-02-11 14:00:00
Location Street Address
21 Old Country Road
Location City Name
Water Mill
Location County Name
Suffolk
Location State Abbreviation
NY
Location Postal Code
11976
Location Latitude
40.907022
Location Longitude
-72.361801
Nrc Rpt Datetime
2015-02-11 16:20:00
Nrc Rpt Num
1107916
Commodity Released Type
Natural Gas
Unintentional Release
0.1
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
2
Injure
2
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2015-02-11 14:28:00
On Site Datetime
2015-02-11 14:28:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Residential Building (One Story Home)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Other
System Part Details
Inside Meter And Regulator Set And Internal Piping
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Leak
Leak Type
Other
Leak Type Other
Third Party Work Caused Damage
Class Location Type
Class 4 Location
Est Cost Oper Paid
500000.0
Est Cost Prop Damage
0.0
Est Cost Emergency
0.0
Est Cost Other
0.0
Est Cost Unintentional Release
50.0
Prpty
500050.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Accident Psig
54.0
Normal Psig
54.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident was not the result of any operation that the control room can detect under present operating conditions and alarms.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
Renovation Work Was Ongoing And The Workers Reported To The Police That They Had Cut Through Internal Piping Immediately Prior To The Incident.
Preparer Name
C****** B*****
Preparer Title
Prin Prog Mgr Federal Programs
Preparer Email
C*************@n***********.com
Preparer Telephone
6317703549
Authorizer Name
C****** B*****
Authorizer Title
Prin Prog Mgr- Federal Programs
Authorizer Telephone
6317703549
Authorizer Email
C*************@n***********.com
Narrative
Based on the preliminary investigation it appears the gas leak on piping located in the basement of the premises, renovation work was ongoing and the workers reported to the police that they had cut through internal piping immediately prior to the incident. The company conducted a pressure test on the gas service line to the premises following the incident; no leaks were detected on the service line. There is no relevant leak history in the area or other indication of issues with the company's gas facilities. The account was inactive at the time of the incident
| Occurred At | 2015-02-11 14:28:00 |
|---|---|
| Year | 2015 |
| Report Received Date | 2016-02-19 00:00:00 |
| Iyear | 2015.0 |
| Report Number | 20160016.0 |
| Supplemental Number | 16608.0 |
| Report Type | Supplemental Final |
| Operator Id | 11713 PHMSA Enforcement |
| Name | Keyspan Energy Delivery - Long Island |
| Operator Street Address | 175 East Old Country Road |
| Operator City Name | Hicksville |
| Operator State Abbreviation | NY |
| Operator Postal Code | 11801 |
| Local Datetime | 2015-02-11 14:00:00 |
| Location Street Address | 21 Old Country Road |
| Location City Name | Water Mill |
| Location County Name | Suffolk |
| Location State Abbreviation | NY |
| Location Postal Code | 11976 |
| Location Latitude | 40.907022 Google Maps OpenStreetMap |
| Location Longitude | -72.361801 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2015-02-11 16:20:00 |
| Nrc Rpt Num | 1107916 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 0.1 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | Yes |
| Num Emp Injuries | 0 |
| Num Contr Injuries | 0 |
| Num Er Injuries | 0 |
| Num Worker Injuries | 0 |
| Num Gp Injuries | 2 |
| Injure | 2 |
| Ignite Ind | Yes |
| Explode Ind | No |
| Num Pub Evacuated | 0.0 |
| Incident Identified Datetime | 2015-02-11 14:28:00 |
| On Site Datetime | 2015-02-11 14:28:00 |
| Federal | No |
| Location Type | Private Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Other |
| Incident Area Details | Residential Building (One Story Home) |
| Crossing | No |
| Pipe Facility Type | Investor Owned |
| System Part Involved | Other |
| System Part Details | Inside Meter And Regulator Set And Internal Piping |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Third Party Work Caused Damage |
| Class Location Type | Class 4 Location |
| Est Cost Oper Paid | 500000.0 |
| Est Cost Prop Damage | 0.0 |
| Est Cost Emergency | 0.0 |
| Est Cost Other | 0.0 |
| Est Cost Unintentional Release | 50.0 |
| Prpty | 500050.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 1.0 |
| Accident Psig | 54.0 |
| Normal Psig | 54.0 |
| Mop Psig | 60.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Accident Identifier | Notification From Emergency Responder |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The incident was not the result of any operation that the control room can detect under present operating conditions and alarms. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Other Outside Force Damage |
| Cause Details | Other Outside Force Damage |
| Outside Force Type | Other Outside Force Damage |
| Osf Other Details | Renovation Work Was Ongoing And The Workers Reported To The Police That They Had Cut Through Internal Piping Immediately Prior To The Incident. |
| Preparer Name | C****** B***** |
| Preparer Title | Prin Prog Mgr Federal Programs |
| Preparer Email | C*************@n***********.com |
| Preparer Telephone | 6317703549 |
| Authorizer Name | C****** B***** |
| Authorizer Title | Prin Prog Mgr- Federal Programs |
| Authorizer Telephone | 6317703549 |
| Authorizer Email | C*************@n***********.com |
| Narrative | Based on the preliminary investigation it appears the gas leak on piping located in the basement of the premises, renovation work was ongoing and the workers reported to the police that they had cut through internal piping immediately prior to the incident. The company conducted a pressure test on the gas service line to the premises following the incident; no leaks were detected on the service line. There is no relevant leak history in the area or other indication of issues with the company's gas facilities. The account was inactive at the time of the incident |
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