GD incident on 2015-12-16 — AZ

Operator
Graham County Util Inc
Cause
Equipment Failure
Commodity
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,000
Incident datetime
2015-12-16 07:30
Report number
Location
AZ, GRAHAM
Narrative
It was determined that a 2" axial flow regulator at thatcher tap # 14-2 had frozen in the unseasonably cold weather, causing loss of line pack and eventual outage to 1972 consumers in the thatcher area.
Detailed record list
Occurred At
2015-12-16 07:30:00
Year
2015
Report Received Date
2016-02-01 00:00:00
Iyear
2015.0
Report Number
20160008.0
Supplemental Number
16232.0
Report Type
Original Final
Operator Id
Name
Graham County Util Inc
Operator Street Address
9 West Center
Operator City Name
Pima
Operator State Abbreviation
AZ
Operator Postal Code
85543
Local Datetime
2015-12-16 06:30:00
Location Street Address
Thatcher
Location City Name
Thatcher
Location County Name
Graham
Location State Abbreviation
AZ
Location Postal Code
85552
Location Latitude
Location Longitude
-109.7514824
Nrc Rpt Datetime
2015-12-16 08:23:00
Nrc Rpt Num
Unintentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2015-12-16 07:30:00
On Site Datetime
2015-12-16 08:00:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Cooperative
System Part Involved
District Regulator/metering Station
Material Involved
Other
Material Details
2" Axial Flow Regulator
Release Type
Other
Release Type Details
Not A Release, Regulator Froze Up
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
4000.0
Est Cost Emergency
68880.0
Est Cost Other
7485.0
Est Cost Other Details
Wages Etc. From Other Local Gas Companies
Est Cost Unintentional Release
0.0
Prpty
80365.0
Commercial Affected
110.0
Industrial Affected
0.0
Residences Affected
1832.0
Accident Psig
0.0
Normal Psig
50.0
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Pressure Regulator Ind
Yes
Preparer Name
W** R*******
Preparer Title
Gas Superintendent
Preparer Email
W***@g**.coop
Preparer Telephone
(928)485-2451
Preparer Fax
(928)485-9491
Authorizer Name
J**** H*****
Authorizer Title
Gas Superintendant
Authorizer Telephone
(928) 651-6034
Authorizer Email
J**********@g**.coop
Narrative
It was determined that a 2" axial flow regulator at thatcher tap # 14-2 had frozen in the unseasonably cold weather, causing loss of line pack and eventual outage to 1972 consumers in the thatcher area.
Occurred At 2015-12-16 07:30:00
Year 2015
Report Received Date 2016-02-01 00:00:00
Iyear 2015.0
Report Number 20160008.0
Supplemental Number 16232.0
Report Type Original Final
Operator Id 6484 PHMSA Enforcement
Name Graham County Util Inc
Operator Street Address 9 West Center
Operator City Name Pima
Operator State Abbreviation AZ
Operator Postal Code 85543
Local Datetime 2015-12-16 06:30:00
Location Street Address Thatcher
Location City Name Thatcher
Location County Name Graham
Location State Abbreviation AZ
Location Postal Code 85552
Location Latitude 32.8302374 Google Maps OpenStreetMap
Location Longitude -109.7514824 Google Maps OpenStreetMap
Nrc Rpt Datetime 2015-12-16 08:23:00
Nrc Rpt Num 1135942 NRC Report How to search
Unintentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2015-12-16 07:30:00
On Site Datetime 2015-12-16 08:00:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing No
Pipe Facility Type Cooperative
System Part Involved District Regulator/metering Station
Material Involved Other
Material Details 2" Axial Flow Regulator
Release Type Other
Release Type Details Not A Release, Regulator Froze Up
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 4000.0
Est Cost Emergency 68880.0
Est Cost Other 7485.0
Est Cost Other Details Wages Etc. From Other Local Gas Companies
Est Cost Unintentional Release 0.0
Prpty 80365.0
Commercial Affected 110.0
Industrial Affected 0.0
Residences Affected 1832.0
Accident Psig 0.0
Normal Psig 50.0
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Pressure Regulator Ind Yes
Preparer Name W** R*******
Preparer Title Gas Superintendent
Preparer Email W***@g**.coop
Preparer Telephone (928)485-2451
Preparer Fax (928)485-9491
Authorizer Name J**** H*****
Authorizer Title Gas Superintendant
Authorizer Telephone (928) 651-6034
Authorizer Email J**********@g**.coop
Narrative It was determined that a 2" axial flow regulator at thatcher tap # 14-2 had frozen in the unseasonably cold weather, causing loss of line pack and eventual outage to 1972 consumers in the thatcher area.

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