HL incident on 2015-11-20 — OK

Operator
Chaparral Energy, Llc
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25
Incident datetime
2015-11-20 09:30
Report number
Location
OK
Narrative
On friday, november 20 at 09:30 chaparral received a call from its contractor that a leak had developed on a one inch tubing connection feeding a pressure transmitter. The contractor was instructed to immediately close the valve feeding the pressure transmitter. At 10:45 a chaparral representative arrived at location to verify the leak. At 12:00 a chaparral representative ordered replacement parts to replace the faulty component. On monday, november 23 at 11:00 a chaparral representative replaced the faulty component. At 12:30 the one inch tubing feeding the pressure transmitter was put back into service without incident. The leak caused no personnel, property, or environmental damage and did not affect a high consequence area.
Detailed record list
Report Received Date
2015-12-21 00:00:00
Iyear
2015
Report Number
20150469
Supplemental Number
21490
Report Type
Supplemental Final
Operator Id
Name
Chaparral Energy, Llc
Operator Street Address
701 Cedar Lake Blvd
Operator City Name
Oklahoma City
Operator State Abbreviation
OK
Operator Postal Code
73114
Local Datetime
2015-11-20 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
1181
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-11-20 09:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
1" Tubing Connection Failed. Tubing Was Isolated And Connection Repaired
On Site Datetime
2015-11-20 09:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Coffeyville Co2 Pipeline
Segment Name
F2269
Onshore State Abbreviation
Ok
Onshore Postal Code
74652
Onshore City Name
Not Within A Municipality
Onshore County Name
Osage
Designated Location
Milepost/valve Station
Designated Name
Mlv 13
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2800
Est Cost Prop Damage
25
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2825
Accident Psig
1235
Mop Psig
1671
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Phmsa
Length Segment Isolated
4
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Other
Other Non Threaded Details
On 1" Tubing A Ferrule Had Failed To Properly Crimp The Tubing At A "t" Fitting.
Additional Defect Ind
Yes
Additional Installation Ind
Yes
Preparer Name
C*** N D******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
C***********@c**************.com
Preparer Telephone
405-426-4470
Preparer Fax
405-425-8470
Prepared Date
2016-07-06 00:00:00
Authorizer Name
C**** C*******
Authorizer Telephone
405-426-4335
Authorizer Title
Pipeline Foreman
Authorizer Email
C*************@c**************.com
Narrative
On friday, november 20 at 09:30 chaparral received a call from its contractor that a leak had developed on a one inch tubing connection feeding a pressure transmitter. The contractor was instructed to immediately close the valve feeding the pressure transmitter. At 10:45 a chaparral representative arrived at location to verify the leak. At 12:00 a chaparral representative ordered replacement parts to replace the faulty component. On monday, november 23 at 11:00 a chaparral representative replaced the faulty component. At 12:30 the one inch tubing feeding the pressure transmitter was put back into service without incident. The leak caused no personnel, property, or environmental damage and did not affect a high consequence area.
Report Received Date 2015-12-21 00:00:00
Iyear 2015
Report Number 20150469
Supplemental Number 21490
Report Type Supplemental Final
Operator Id 31672 PHMSA Enforcement
Name Chaparral Energy, Llc
Operator Street Address 701 Cedar Lake Blvd
Operator City Name Oklahoma City
Operator State Abbreviation OK
Operator Postal Code 73114
Local Datetime 2015-11-20 09:30:00
Location Latitude 36.79693 Google Maps OpenStreetMap
Location Longitude -96.663049 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 1181
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-11-20 09:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain 1" Tubing Connection Failed. Tubing Was Isolated And Connection Repaired
On Site Datetime 2015-11-20 09:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Coffeyville Co2 Pipeline
Segment Name F2269
Onshore State Abbreviation Ok
Onshore Postal Code 74652
Onshore City Name Not Within A Municipality
Onshore County Name Osage
Designated Location Milepost/valve Station
Designated Name Mlv 13
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 2800
Est Cost Prop Damage 25
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2825
Accident Psig 1235
Mop Psig 1671
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Phmsa
Length Segment Isolated 4
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Other
Other Non Threaded Details On 1" Tubing A Ferrule Had Failed To Properly Crimp The Tubing At A "t" Fitting.
Additional Defect Ind Yes
Additional Installation Ind Yes
Preparer Name C*** N D******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email C***********@c**************.com
Preparer Telephone 405-426-4470
Preparer Fax 405-425-8470
Prepared Date 2016-07-06 00:00:00
Authorizer Name C**** C*******
Authorizer Telephone 405-426-4335
Authorizer Title Pipeline Foreman
Authorizer Email C*************@c**************.com
Narrative On friday, november 20 at 09:30 chaparral received a call from its contractor that a leak had developed on a one inch tubing connection feeding a pressure transmitter. The contractor was instructed to immediately close the valve feeding the pressure transmitter. At 10:45 a chaparral representative arrived at location to verify the leak. At 12:00 a chaparral representative ordered replacement parts to replace the faulty component. On monday, november 23 at 11:00 a chaparral representative replaced the faulty component. At 12:30 the one inch tubing feeding the pressure transmitter was put back into service without incident. The leak caused no personnel, property, or environmental damage and did not affect a high consequence area.

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