HL incident on 2015-12-25 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2015-12-25 23:00
Report number
Location
TX
Narrative
On nov. 25 at approximately 2300 hrs., after operations completed routine bi-annual esd testing, the station was being brought back into service. A company I &e tech noticed oil coming from the side of the control valve on the primary meter run. The meter was immediately shut in and the alternate meter was brought on line at approximately 2305 hrs. Investigation found cover of the packing seal leaking on the control valve. The primary control valve had the packing seal repaired and brought back on line and in service at 1300 hrs. On dec 2nd
Detailed record list
Report Received Date
2015-12-17 00:00:00
Iyear
2015
Report Number
20150466
Supplemental Number
20998
Report Type
Original Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-11-25 23:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-12-25 23:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Already Shut Down For Routine Maintenance, Leak Occurred During Startup
On Site Datetime
2015-11-25 23:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Rio Bravo Crude Pipeline
Segment Name
George West Pump Station
Onshore State Abbreviation
Tx
Onshore Postal Code
78022
Onshore City Name
George West
Onshore County Name
Live Oak
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
40
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
12000
Est Cost Other
0
Prpty
13540
Accident Psig
300
Mop Psig
1100
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Packing Cover On Control Valve Was Leaking
Additional Breakdown Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Packing Seal Leak
Preparer Name
W****** M****
Preparer Title
Manager Intrastate Compliance
Preparer Email
B*********@e*************.com
Preparer Telephone
713-9896460
Prepared Date
2015-12-17 00:00:00
Authorizer Name
D**** N******
Authorizer Telephone
7139897232
Authorizer Title
Director Regulatory Compliance
Authorizer Email
D************@e*************.com
Narrative
On nov. 25 at approximately 2300 hrs., after operations completed routine bi-annual esd testing, the station was being brought back into service. A company I &e tech noticed oil coming from the side of the control valve on the primary meter run. The meter was immediately shut in and the alternate meter was brought on line at approximately 2305 hrs. Investigation found cover of the packing seal leaking on the control valve. The primary control valve had the packing seal repaired and brought back on line and in service at 1300 hrs. On dec 2nd
Report Received Date 2015-12-17 00:00:00
Iyear 2015
Report Number 20150466
Supplemental Number 20998
Report Type Original Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-11-25 23:00:00
Location Latitude 28.3448 Google Maps OpenStreetMap
Location Longitude -98.1212 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-12-25 23:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Already Shut Down For Routine Maintenance, Leak Occurred During Startup
On Site Datetime 2015-11-25 23:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Rio Bravo Crude Pipeline
Segment Name George West Pump Station
Onshore State Abbreviation Tx
Onshore Postal Code 78022
Onshore City Name George West
Onshore County Name Live Oak
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 40
Est Cost Prop Damage 1500
Est Cost Emergency 0
Est Cost Environmental 12000
Est Cost Other 0
Prpty 13540
Accident Psig 300
Mop Psig 1100
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Packing Cover On Control Valve Was Leaking
Additional Breakdown Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Packing Seal Leak
Preparer Name W****** M****
Preparer Title Manager Intrastate Compliance
Preparer Email B*********@e*************.com
Preparer Telephone 713-9896460
Prepared Date 2015-12-17 00:00:00
Authorizer Name D**** N******
Authorizer Telephone 7139897232
Authorizer Title Director Regulatory Compliance
Authorizer Email D************@e*************.com
Narrative On nov. 25 at approximately 2300 hrs., after operations completed routine bi-annual esd testing, the station was being brought back into service. A company I &e tech noticed oil coming from the side of the control valve on the primary meter run. The meter was immediately shut in and the alternate meter was brought on line at approximately 2305 hrs. Investigation found cover of the packing seal leaking on the control valve. The primary control valve had the packing seal repaired and brought back on line and in service at 1300 hrs. On dec 2nd

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