HL incident on 2015-11-02 — TX

Operator
Wyoming Pipeline Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2015-11-02 09:30
Report number
Location
TX
Narrative
Leak was discovered by air patrol that called mccc, wpc personnel dispatched to site, crude migrated into surface water of a natural spring, a duck was contaminated in oil as discovered by US forest service personnel and decontaminated. Contaminated soil and water were remediated by vac truck and absorbent, contaminated soil was removed to a remediation site and new soil was placed in the excavation.
Detailed record list
Report Received Date
2015-12-11 00:00:00
Iyear
2015
Report Number
20150457
Supplemental Number
22912
Report Type
Supplemental Final
Operator Id
Name
Wyoming Pipeline Company
Operator Street Address
825 Town & Country Lane
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2015-11-02 09:30:00
Location Latitude
Location Longitude
-104.9547281
Commodity Released Type
Crude Oil
Unintentional Release Bbls
20
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-11-02 09:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Out Of Service At Time Of Accident
On Site Datetime
2015-11-02 10:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wpc - Thunder Creek Station
Segment Name
Thunder Creek To Clareton Line
Onshore State Abbreviation
Wy
Onshore Postal Code
82701-0000
Onshore City Name
Not Within A Municipality
Onshore County Name
Weston County, Wyoming
Designated Location
Milepost/valve Station
Designated Name
Usda Nat'l Gr
Federal
Yes
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
34
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.219
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Cold Applied Tape
Installation Year
1976
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
Yes
Birds Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Wildlife Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
2
Rel Water Name
Unknown
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
250
Est Cost Gas Released
800
Est Cost Prop Damage
100
Est Cost Emergency
7185
Est Cost Environmental
12615
Est Cost Other
500
Est Cost Other Details
U.s Forest Service National Grasslands Reseeding
Prpty
21450
Accident Psig
0
Mop Psig
535
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was too small to be discovered by the scada system
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2015
Close Interval Survey Year
2014
Other Cp Survey Year
2014
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
W****** M********
Preparer Title
Compliance Consultant
Preparer Email
W*****@c**.net
Preparer Telephone
405-820-1304
Prepared Date
2017-12-08 00:00:00
Authorizer Name
N***** H******
Authorizer Telephone
307-746-9479
Authorizer Title
Pipeline Director
Authorizer Email
N*******@w****.com
Narrative
Leak was discovered by air patrol that called mccc, wpc personnel dispatched to site, crude migrated into surface water of a natural spring, a duck was contaminated in oil as discovered by US forest service personnel and decontaminated. Contaminated soil and water were remediated by vac truck and absorbent, contaminated soil was removed to a remediation site and new soil was placed in the excavation.
Report Received Date 2015-12-11 00:00:00
Iyear 2015
Report Number 20150457
Supplemental Number 22912
Report Type Supplemental Final
Operator Id 32537 PHMSA Enforcement
Name Wyoming Pipeline Company
Operator Street Address 825 Town & Country Lane
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2015-11-02 09:30:00
Location Latitude 43.67297971 Google Maps OpenStreetMap
Location Longitude -104.9547281 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 20
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-11-02 09:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Out Of Service At Time Of Accident
On Site Datetime 2015-11-02 10:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wpc - Thunder Creek Station
Segment Name Thunder Creek To Clareton Line
Onshore State Abbreviation Wy
Onshore Postal Code 82701-0000
Onshore City Name Not Within A Municipality
Onshore County Name Weston County, Wyoming
Designated Location Milepost/valve Station
Designated Name Usda Nat'l Gr
Federal Yes
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 34
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.219
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Cold Applied Tape
Installation Year 1976
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind Yes
Birds Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Wildlife Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 2
Rel Water Name Unknown
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 250
Est Cost Gas Released 800
Est Cost Prop Damage 100
Est Cost Emergency 7185
Est Cost Environmental 12615
Est Cost Other 500
Est Cost Other Details U.s Forest Service National Grasslands Reseeding
Prpty 21450
Accident Psig 0
Mop Psig 535
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was too small to be discovered by the scada system
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2015
Close Interval Survey Year 2014
Other Cp Survey Year 2014
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name W****** M********
Preparer Title Compliance Consultant
Preparer Email W*****@c**.net
Preparer Telephone 405-820-1304
Prepared Date 2017-12-08 00:00:00
Authorizer Name N***** H******
Authorizer Telephone 307-746-9479
Authorizer Title Pipeline Director
Authorizer Email N*******@w****.com
Narrative Leak was discovered by air patrol that called mccc, wpc personnel dispatched to site, crude migrated into surface water of a natural spring, a duck was contaminated in oil as discovered by US forest service personnel and decontaminated. Contaminated soil and water were remediated by vac truck and absorbent, contaminated soil was removed to a remediation site and new soil was placed in the excavation.

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