HL incident on 2014-09-25 — ND

Operator
Dakota Gasification Company
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2014-09-25 01:05
Report number
Location
ND
Narrative
After general work, the control room for the CO2 pipeline initiated efforts to start pump ga7411. The board operator called for 40% open on flow valve fv74056. During startup, pressures built to 3001 psi without the valve opening. System alarms, shuts down is initiated by the board operator. The sequence is tried again, with the same results. E&I are dispatched to find the cause, which is determined to be a faulty servo driver. During investigation of ga7411, psv 74050 was found with a micro (pin hole) leak emitting from the side body. The psv was isolated and changed with a like psv by maintenance. Subsequent examination found the valve body o-ring on the inspection port wsas bad. The o ring was changed, psv tested and placed in reserve stock. Estimate gas losses: - hydrogen sulfide 10 lbs; carbon dioxide 800 lbs = 72 gallons
Detailed record list
Report Received Date
2015-12-10 00:00:00
Iyear
2014
Report Number
20150451
Supplemental Number
22581
Report Type
Supplemental Final
Operator Id
Name
Dakota Gasification Company
Operator Street Address
1717 East Interstate Avenue
Operator City Name
Bismarck
Operator State Abbreviation
ND
Operator Postal Code
58503-0564
Local Datetime
2014-09-25 01:05:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
1
Intentional Release Bbls
1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2014-09-25 01:05:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pressure Reduction; Psv Replaced On Vent Line
On Site Datetime
2014-09-25 07:00:00
Nrc Rpt Datetime
2014-09-25 15:57:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Dakota Gasification
Segment Name
Tioga Station
Onshore State Abbreviation
Nd
Onshore Postal Code
58852
Onshore City Name
Tioga
Onshore County Name
Williams
Designated Location
Milepost/valve Station
Designated Name
Valvestation
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2014
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
500
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2000
Accident Psig
3001
Mop Psig
3100
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Additional Installation Ind
Yes
Preparer Name
C***** O******
Preparer Title
Pipeline Superintendent
Preparer Email
C******@b***.com
Preparer Telephone
7018736155
Prepared Date
2017-08-21 00:00:00
Authorizer Name
C***** O******
Authorizer Telephone
7018736155
Authorizer Title
Pipeline Superintendent
Authorizer Email
C******@b***.com
Narrative
After general work, the control room for the CO2 pipeline initiated efforts to start pump ga7411. The board operator called for 40% open on flow valve fv74056. During startup, pressures built to 3001 psi without the valve opening. System alarms, shuts down is initiated by the board operator. The sequence is tried again, with the same results. E&I are dispatched to find the cause, which is determined to be a faulty servo driver. During investigation of ga7411, psv 74050 was found with a micro (pin hole) leak emitting from the side body. The psv was isolated and changed with a like psv by maintenance. Subsequent examination found the valve body o-ring on the inspection port wsas bad. The o ring was changed, psv tested and placed in reserve stock. Estimate gas losses: - hydrogen sulfide 10 lbs; carbon dioxide 800 lbs = 72 gallons
Report Received Date 2015-12-10 00:00:00
Iyear 2014
Report Number 20150451
Supplemental Number 22581
Report Type Supplemental Final
Operator Id 515 PHMSA Enforcement
Name Dakota Gasification Company
Operator Street Address 1717 East Interstate Avenue
Operator City Name Bismarck
Operator State Abbreviation ND
Operator Postal Code 58503-0564
Local Datetime 2014-09-25 01:05:00
Location Latitude 48.3975 Google Maps OpenStreetMap
Location Longitude -102.901 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 1
Intentional Release Bbls 1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2014-09-25 01:05:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pressure Reduction; Psv Replaced On Vent Line
On Site Datetime 2014-09-25 07:00:00
Nrc Rpt Datetime 2014-09-25 15:57:00
Nrc Rpt Num 1096486 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Dakota Gasification
Segment Name Tioga Station
Onshore State Abbreviation Nd
Onshore Postal Code 58852
Onshore City Name Tioga
Onshore County Name Williams
Designated Location Milepost/valve Station
Designated Name Valvestation
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2014
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 500
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 2000
Accident Psig 3001
Mop Psig 3100
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Additional Installation Ind Yes
Preparer Name C***** O******
Preparer Title Pipeline Superintendent
Preparer Email C******@b***.com
Preparer Telephone 7018736155
Prepared Date 2017-08-21 00:00:00
Authorizer Name C***** O******
Authorizer Telephone 7018736155
Authorizer Title Pipeline Superintendent
Authorizer Email C******@b***.com
Narrative After general work, the control room for the CO2 pipeline initiated efforts to start pump ga7411. The board operator called for 40% open on flow valve fv74056. During startup, pressures built to 3001 psi without the valve opening. System alarms, shuts down is initiated by the board operator. The sequence is tried again, with the same results. E&I are dispatched to find the cause, which is determined to be a faulty servo driver. During investigation of ga7411, psv 74050 was found with a micro (pin hole) leak emitting from the side body. The psv was isolated and changed with a like psv by maintenance. Subsequent examination found the valve body o-ring on the inspection port wsas bad. The o ring was changed, psv tested and placed in reserve stock. Estimate gas losses: - hydrogen sulfide 10 lbs; carbon dioxide 800 lbs = 72 gallons

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