HL incident on 2015-11-09 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$337,771
Incident datetime
2015-11-09 08:00
Report number
Location
TX
Narrative
At approximately 8:00 am on november 9, 2015, a contractor discovered approximately 3 ounces of oil weeping from the line 2 valve at mp 1005.31 near cohasset, mn. The oil was wiped up and the control center was notified of the situation. Due to the valve not actively leaking, line 2 continued to operate and the valve was closely monitored. While the valve was being monitored, multiple discussions with enbridge sme's and the valve manufacturer took place to discuss repair options. Once the final repair plan was decided upon, notification was made to the nrc as the cost for the repair would exceed the notification threshold. In order to safely inspect and repair the valve, stopple equipment was utilized for isolation. During inspection of the valve, it was found that the o-ring required replacement due to exceeding its useful life. In addition to replacing the o-ring, new bonnet studs and nuts were installed. There was no contaminated soil associated with this incident.
Detailed record list
Report Received Date
2015-12-08 00:00:00
Iyear
2015
Report Number
20150448
Supplemental Number
20966
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-11-09 08:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.01
Recovered Bbls
0.01
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-11-09 08:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Was Not Actively Leaking Therefore No Shutdown Requested
On Site Datetime
2015-11-09 08:00:00
Nrc Rpt Datetime
2015-11-12 11:02:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Line 2
Segment Name
Line 2 Mp1005.31
Onshore State Abbreviation
Mn
Onshore Postal Code
55721
Onshore City Name
Cohasset
Onshore County Name
Itasca
Designated Location
Milepost/valve Station
Designated Name
1005.31
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
14
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
1973
Manufactured Year
1973
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
337771
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
339771
Accident Psig
287
Mop Psig
717
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
49050
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Neither the operator nor the control center had involvement in this incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Exceeded Useful Life
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-394-1564
Prepared Date
2015-12-08 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Manager Us Pipelines Compliance
Authorizer Email
R***********@e*******.com
Narrative
At approximately 8:00 am on november 9, 2015, a contractor discovered approximately 3 ounces of oil weeping from the line 2 valve at mp 1005.31 near cohasset, mn. The oil was wiped up and the control center was notified of the situation. Due to the valve not actively leaking, line 2 continued to operate and the valve was closely monitored. While the valve was being monitored, multiple discussions with enbridge sme's and the valve manufacturer took place to discuss repair options. Once the final repair plan was decided upon, notification was made to the nrc as the cost for the repair would exceed the notification threshold. In order to safely inspect and repair the valve, stopple equipment was utilized for isolation. During inspection of the valve, it was found that the o-ring required replacement due to exceeding its useful life. In addition to replacing the o-ring, new bonnet studs and nuts were installed. There was no contaminated soil associated with this incident.
Report Received Date 2015-12-08 00:00:00
Iyear 2015
Report Number 20150448
Supplemental Number 20966
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-11-09 08:00:00
Location Latitude 47.261205 Google Maps OpenStreetMap
Location Longitude -93.591633 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.01
Recovered Bbls 0.01
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-11-09 08:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Was Not Actively Leaking Therefore No Shutdown Requested
On Site Datetime 2015-11-09 08:00:00
Nrc Rpt Datetime 2015-11-12 11:02:00
Nrc Rpt Num 1133254 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Line 2
Segment Name Line 2 Mp1005.31
Onshore State Abbreviation Mn
Onshore Postal Code 55721
Onshore City Name Cohasset
Onshore County Name Itasca
Designated Location Milepost/valve Station
Designated Name 1005.31
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 14
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year 1973
Manufactured Year 1973
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 337771
Est Cost Emergency 2000
Est Cost Environmental 0
Est Cost Other 0
Prpty 339771
Accident Psig 287
Mop Psig 717
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 49050
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Neither the operator nor the control center had involvement in this incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Exceeded Useful Life
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-394-1564
Prepared Date 2015-12-08 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Manager Us Pipelines Compliance
Authorizer Email R***********@e*******.com
Narrative At approximately 8:00 am on november 9, 2015, a contractor discovered approximately 3 ounces of oil weeping from the line 2 valve at mp 1005.31 near cohasset, mn. The oil was wiped up and the control center was notified of the situation. Due to the valve not actively leaking, line 2 continued to operate and the valve was closely monitored. While the valve was being monitored, multiple discussions with enbridge sme's and the valve manufacturer took place to discuss repair options. Once the final repair plan was decided upon, notification was made to the nrc as the cost for the repair would exceed the notification threshold. In order to safely inspect and repair the valve, stopple equipment was utilized for isolation. During inspection of the valve, it was found that the o-ring required replacement due to exceeding its useful life. In addition to replacing the o-ring, new bonnet studs and nuts were installed. There was no contaminated soil associated with this incident.

All rights reserved. Copyright © by ClearPHMSA