HL incident on 2015-11-14 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-11-14 07:45
Report number
Location
TX
Narrative
Operators performed maintenance on the vertical strainer baskets on the meter skid and returned the skid to operation. The strainer's safety bleed valve plug was not re-installed prior to the return of equipment to operation. When a movement of gasoline was made on the meter skid, approximately 57 gallons of gasoline was released from the two 1/16" orifices on the safety bleed valve. The pipeline was then shut down and isolated. Released product was remediated, the plug reinstalled, the equipment leak tested, and the skid brought back into service. An equipment-specific maintenance procedure was written to prevent reoccurrence of this release.
Detailed record list
Report Received Date
2015-12-08 00:00:00
Iyear
2015
Report Number
20150447
Supplemental Number
20965
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-11-14 07:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
1.4
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-11-14 07:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-11-14 07:45:00
Restart Datetime
2015-11-14 14:00:00
On Site Datetime
2015-11-14 07:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Beaumont Marine West Export Meter Skid
Segment Name
Beaumont Terminal To Beaumont Marine West #1
Onshore State Abbreviation
Tx
Onshore Postal Code
77720
Onshore City Name
Beaumont
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Bmw Meter
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Bleed Plug Not Replaced
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
77
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
3000
Est Cost Other
0
Prpty
3077
Accident Psig
74
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller actions did not contribute to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related No Proc Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
No
Preparer Name
M*** P*****
Preparer Title
Sr. Compliance Specialist
Preparer Email
M*******@e****.com
Preparer Telephone
713-381-5897
Prepared Date
2015-12-08 00:00:00
Authorizer Name
M*** P*****
Authorizer Telephone
713-381-5897
Authorizer Title
Sr. Compliance Specialist
Authorizer Email
M*******@e****.com
Narrative
Operators performed maintenance on the vertical strainer baskets on the meter skid and returned the skid to operation. The strainer's safety bleed valve plug was not re-installed prior to the return of equipment to operation. When a movement of gasoline was made on the meter skid, approximately 57 gallons of gasoline was released from the two 1/16" orifices on the safety bleed valve. The pipeline was then shut down and isolated. Released product was remediated, the plug reinstalled, the equipment leak tested, and the skid brought back into service. An equipment-specific maintenance procedure was written to prevent reoccurrence of this release.
Report Received Date 2015-12-08 00:00:00
Iyear 2015
Report Number 20150447
Supplemental Number 20965
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-11-14 07:45:00
Location Latitude 30.030029 Google Maps OpenStreetMap
Location Longitude -94.041199 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 1.4
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-11-14 07:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-11-14 07:45:00
Restart Datetime 2015-11-14 14:00:00
On Site Datetime 2015-11-14 07:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Beaumont Marine West Export Meter Skid
Segment Name Beaumont Terminal To Beaumont Marine West #1
Onshore State Abbreviation Tx
Onshore Postal Code 77720
Onshore City Name Beaumont
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Bmw Meter
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Bleed Plug Not Replaced
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 77
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 3000
Est Cost Other 0
Prpty 3077
Accident Psig 74
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller actions did not contribute to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related No Proc Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind No
Preparer Name M*** P*****
Preparer Title Sr. Compliance Specialist
Preparer Email M*******@e****.com
Preparer Telephone 713-381-5897
Prepared Date 2015-12-08 00:00:00
Authorizer Name M*** P*****
Authorizer Telephone 713-381-5897
Authorizer Title Sr. Compliance Specialist
Authorizer Email M*******@e****.com
Narrative Operators performed maintenance on the vertical strainer baskets on the meter skid and returned the skid to operation. The strainer's safety bleed valve plug was not re-installed prior to the return of equipment to operation. When a movement of gasoline was made on the meter skid, approximately 57 gallons of gasoline was released from the two 1/16" orifices on the safety bleed valve. The pipeline was then shut down and isolated. Released product was remediated, the plug reinstalled, the equipment leak tested, and the skid brought back into service. An equipment-specific maintenance procedure was written to prevent reoccurrence of this release.

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