HL incident on 2015-11-09 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Excavation Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$125,000
Incident datetime
2015-11-09 15:30
Report number
Location
OK
Narrative
While direction drilling and pulling back electrical conduit inside magellan's rosemount tank farm facility, the reamer nicked the bottom of the line serving tank 842, which released product to the soil. The damaged pipe was cut out and replaced with approximately 4 feet of new, pre-tested 12.75" o.D. By 0.375 wall API 5l x52 grade pipe and the line was returned to service. Approximately 220 cubic yards of impacted soil was remediated. Note: the puncture size was approximately 0.75" x 0.75". Part c, #6 of this report would not accept decimals and erroneously lists the puncture as 75" x 75".
Detailed record list
Report Received Date
2015-12-07 00:00:00
Iyear
2015
Report Number
20150446
Supplemental Number
20964
Report Type
Original Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-11-09 15:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
10.8
Recovered Bbls
10.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-11-09 15:30:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-11-09 16:30:00
Restart Datetime
2015-11-12 14:50:00
On Site Datetime
2015-11-09 15:30:00
Nrc Rpt Datetime
2015-11-09 16:41:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Rosemount Station
Segment Name
Station #568
Onshore State Abbreviation
Mn
Onshore Postal Code
55124
Onshore City Name
Apple Valley
Onshore County Name
Dakota
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Api 5lb X42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Chung Hung Steel Corporation
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2008
Manufactured Year
2007
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
75
Puncture Circum
75
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
687
Est Cost Prop Damage
125000
Est Cost Emergency
2000
Est Cost Environmental
125000
Est Cost Other
0
Prpty
252687
Accident Psig
3
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No official incident investigation was performed, as operations control supervisor determined that controller followed proper procedure for the operations being initiated, and in addition, release volume was significantly below any alarm tolerances. The cpm system monitors the pipeline, not the facility; no cpm alarms were generated.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
Yes
Private Row Ind
Yes
Private Subtype
Private Business
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Electric
One Call Notified Ind
Yes
One Call Ticket Num
152990774
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
71
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-1187
Prepared Date
2015-12-07 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
While direction drilling and pulling back electrical conduit inside magellan's rosemount tank farm facility, the reamer nicked the bottom of the line serving tank 842, which released product to the soil. The damaged pipe was cut out and replaced with approximately 4 feet of new, pre-tested 12.75" o.D. By 0.375 wall API 5l x52 grade pipe and the line was returned to service. Approximately 220 cubic yards of impacted soil was remediated. Note: the puncture size was approximately 0.75" x 0.75". Part c, #6 of this report would not accept decimals and erroneously lists the puncture as 75" x 75".
Report Received Date 2015-12-07 00:00:00
Iyear 2015
Report Number 20150446
Supplemental Number 20964
Report Type Original Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-11-09 15:30:00
Location Latitude 44.73368 Google Maps OpenStreetMap
Location Longitude -93.19464 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 10.8
Recovered Bbls 10.8
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-11-09 15:30:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-11-09 16:30:00
Restart Datetime 2015-11-12 14:50:00
On Site Datetime 2015-11-09 15:30:00
Nrc Rpt Datetime 2015-11-09 16:41:00
Nrc Rpt Num 1132998 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Rosemount Station
Segment Name Station #568
Onshore State Abbreviation Mn
Onshore Postal Code 55124
Onshore City Name Apple Valley
Onshore County Name Dakota
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification Api 5lb X42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Chung Hung Steel Corporation
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2008
Manufactured Year 2007
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 75
Puncture Circum 75
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 687
Est Cost Prop Damage 125000
Est Cost Emergency 2000
Est Cost Environmental 125000
Est Cost Other 0
Prpty 252687
Accident Psig 3
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No official incident investigation was performed, as operations control supervisor determined that controller followed proper procedure for the operations being initiated, and in addition, release volume was significantly below any alarm tolerances. The cpm system monitors the pipeline, not the facility; no cpm alarms were generated.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt Yes
Private Row Ind Yes
Private Subtype Private Business
Excavator Type Contractor
Excavator Equipment Boring
Work Performed Electric
One Call Notified Ind Yes
One Call Ticket Num 152990774
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 71
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-1187
Prepared Date 2015-12-07 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative While direction drilling and pulling back electrical conduit inside magellan's rosemount tank farm facility, the reamer nicked the bottom of the line serving tank 842, which released product to the soil. The damaged pipe was cut out and replaced with approximately 4 feet of new, pre-tested 12.75" o.D. By 0.375 wall API 5l x52 grade pipe and the line was returned to service. Approximately 220 cubic yards of impacted soil was remediated. Note: the puncture size was approximately 0.75" x 0.75". Part c, #6 of this report would not accept decimals and erroneously lists the puncture as 75" x 75".

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