HL incident on 2015-11-04 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-11-04 16:30
Report number
Location
TX
Narrative
Purging a three mile section of 24 inch pipeline with nitrogen. Nitrogen entered the temporary tankage and burped nitrogen and crude oil mist out of the vent.
Detailed record list
Report Received Date
2015-12-02 00:00:00
Iyear
2015
Report Number
20150440
Supplemental Number
21014
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-11-04 16:30:00
Location Latitude
Location Longitude
-121.5874583
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-11-04 16:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Nitrogen Purging / Pipeline Was Not Operating
On Site Datetime
2015-11-04 16:30:00
Nrc Rpt Datetime
2015-11-04 18:13:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
North 20"
Segment Name
Tracy To Windmill Farm
Onshore State Abbreviation
Ca
Onshore Postal Code
95304
Onshore City Name
Not Within A Municipality
Onshore County Name
San Joaquin
Designated Location
Milepost/valve Station
Designated Name
136.1
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Purging To Temp. Tanks
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Tank Type
Atmospheric
Item Involved Details
Temporary Frac Tank For Displacement
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Nitrogen From Pipeline Purge Entered The Temporary Tank And Sprayed Crude Oil Out Of The Vent.
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
9000
Est Cost Environmental
1000
Est Cost Other
0
Prpty
10000
Accident Psig
0
Mop Psig
936
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was being purged by local operating personnel. The pipeline was isolated from the control centers operations.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Inadequate Monitoring
Related Other Ind
Yes
Operation Related Details
Two Of The Personnel Assigned To Man Valves At Frac Tanks To Control Flow When Pig Arrived Were Not Available When Pig Arrived Earlier Than Expected.
Category Type
Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind
No
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
7132411064
Preparer Fax
7132418498
Prepared Date
2015-12-28 00:00:00
Authorizer Name
D****** P****
Authorizer Telephone
7132412035
Authorizer Title
Integrity And Regulatory Srvc Manager
Authorizer Email
D************@s****.com
Narrative
Purging a three mile section of 24 inch pipeline with nitrogen. Nitrogen entered the temporary tankage and burped nitrogen and crude oil mist out of the vent.
Report Received Date 2015-12-02 00:00:00
Iyear 2015
Report Number 20150440
Supplemental Number 21014
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-11-04 16:30:00
Location Latitude 37.75134722 Google Maps OpenStreetMap
Location Longitude -121.5874583 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-11-04 16:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Nitrogen Purging / Pipeline Was Not Operating
On Site Datetime 2015-11-04 16:30:00
Nrc Rpt Datetime 2015-11-04 18:13:00
Nrc Rpt Num 1132600 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name North 20"
Segment Name Tracy To Windmill Farm
Onshore State Abbreviation Ca
Onshore Postal Code 95304
Onshore City Name Not Within A Municipality
Onshore County Name San Joaquin
Designated Location Milepost/valve Station
Designated Name 136.1
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Purging To Temp. Tanks
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Tank Type Atmospheric
Item Involved Details Temporary Frac Tank For Displacement
Installation Year Unknown
Material Involved Carbon Steel
Release Type Other
Release Type Details Nitrogen From Pipeline Purge Entered The Temporary Tank And Sprayed Crude Oil Out Of The Vent.
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 9000
Est Cost Environmental 1000
Est Cost Other 0
Prpty 10000
Accident Psig 0
Mop Psig 936
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was being purged by local operating personnel. The pipeline was isolated from the control centers operations.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Inadequate Monitoring
Related Other Ind Yes
Operation Related Details Two Of The Personnel Assigned To Man Valves At Frac Tanks To Control Flow When Pig Arrived Were Not Available When Pig Arrived Earlier Than Expected.
Category Type Non-Routine Operating Conditions (Abnormal Operations Or Emergencies)
Operator Qualification Ind No
Preparer Name R****** K*****
Preparer Title Regulatory Specialist
Preparer Email R*************@s****.com
Preparer Telephone 7132411064
Preparer Fax 7132418498
Prepared Date 2015-12-28 00:00:00
Authorizer Name D****** P****
Authorizer Telephone 7132412035
Authorizer Title Integrity And Regulatory Srvc Manager
Authorizer Email D************@s****.com
Narrative Purging a three mile section of 24 inch pipeline with nitrogen. Nitrogen entered the temporary tankage and burped nitrogen and crude oil mist out of the vent.

All rights reserved. Copyright © by ClearPHMSA