HL incident on 2015-10-10 — TX

Operator
Gulf State Pipeline Co Inc
Cause
Excavation Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-10-10 10:40
Report number
Location
TX
Narrative
The incident occurred during a pipeline replacement activity when the pipeline system was not active. A trackhoe punctured the old line segment that was being replaced. Only a 2 x 4 inch puncture occurred and 15 barrels of natural gasoline was released into the trench. The trench was immediately bermed to localize the release valves upstream and downstream were blocked. A vacuum truck arrived within 2 hours and collected the released material from the bermed area. Approximately 20 cubic yards of soil exposed to the natural gasoline was excavated and disposed of. No further contamination was detected.
Detailed record list
Report Received Date
2015-12-02 00:00:00
Iyear
2015
Report Number
20150439
Supplemental Number
20951
Report Type
Original
Operator Id
Name
Gulf State Pipeline Co Inc
Operator Street Address
7752 West Fm 418/ Po Box 1636
Operator City Name
Silsbee
Operator State Abbreviation
TX
Operator Postal Code
77656
Local Datetime
2015-10-10 10:40:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Natural Gasoline
Unintentional Release Bbls
15
Recovered Bbls
15
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-10-10 10:40:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-10-10 10:40:00
Restart Datetime
2015-10-10 20:00:00
On Site Datetime
2015-10-10 10:40:00
Nrc Rpt Datetime
2015-10-10 13:38:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Gulf States Pipeline
Segment Name
Section 3 East Side Of Neches River
Onshore State Abbreviation
Tx
Onshore Postal Code
77656
Onshore City Name
Not Within A Municipality
Onshore County Name
Jasper
Designated Location
Milepost/valve Station
Designated Name
11.13 Milepos
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Exposed Pipe During Maintenance
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api 5l X-42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Us Steel
Pipe Coating Type
Coal Tar
Installation Year
1975
Manufactured Year
1974
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
4
Puncture Circum
2
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
0
Est Cost Emergency
1000
Est Cost Environmental
3200
Est Cost Other
0
Est Cost Other Details
Incident Occurred During Replacement Of Pipeline Segment
Prpty
4350
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
15840
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipeline system was not operating at the time of the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Easement
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Liquid Pipeline
One Call Notified Ind
Yes
One Call Ticket Num
Unknown
One Call Center Name
Texas 811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
L**** S****
Preparer Title
Pipeline Manager
Preparer Email
L*****@s************.com
Preparer Telephone
409-385-8300
Preparer Fax
409-385-2453
Prepared Date
2015-12-02 00:00:00
Authorizer Name
R*** F*******
Authorizer Telephone
409-835-8300
Authorizer Title
Vp Manufacturing
Authorizer Email
R*******@s************.com
Narrative
The incident occurred during a pipeline replacement activity when the pipeline system was not active. A trackhoe punctured the old line segment that was being replaced. Only a 2 x 4 inch puncture occurred and 15 barrels of natural gasoline was released into the trench. The trench was immediately bermed to localize the release valves upstream and downstream were blocked. A vacuum truck arrived within 2 hours and collected the released material from the bermed area. Approximately 20 cubic yards of soil exposed to the natural gasoline was excavated and disposed of. No further contamination was detected.
Report Received Date 2015-12-02 00:00:00
Iyear 2015
Report Number 20150439
Supplemental Number 20951
Report Type Original
Operator Id 6911 PHMSA Enforcement
Name Gulf State Pipeline Co Inc
Operator Street Address 7752 West Fm 418/ Po Box 1636
Operator City Name Silsbee
Operator State Abbreviation TX
Operator Postal Code 77656
Local Datetime 2015-10-10 10:40:00
Location Latitude 30.294432 Google Maps OpenStreetMap
Location Longitude -94.111877 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Natural Gasoline
Unintentional Release Bbls 15
Recovered Bbls 15
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-10-10 10:40:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-10-10 10:40:00
Restart Datetime 2015-10-10 20:00:00
On Site Datetime 2015-10-10 10:40:00
Nrc Rpt Datetime 2015-10-10 13:38:00
Nrc Rpt Num 1130551 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Gulf States Pipeline
Segment Name Section 3 East Side Of Neches River
Onshore State Abbreviation Tx
Onshore Postal Code 77656
Onshore City Name Not Within A Municipality
Onshore County Name Jasper
Designated Location Milepost/valve Station
Designated Name 11.13 Milepos
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Exposed Pipe During Maintenance
Depth Of Cover 60
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api 5l X-42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Us Steel
Pipe Coating Type Coal Tar
Installation Year 1975
Manufactured Year 1974
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 4
Puncture Circum 2
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 0
Est Cost Emergency 1000
Est Cost Environmental 3200
Est Cost Other 0
Est Cost Other Details Incident Occurred During Replacement Of Pipeline Segment
Prpty 4350
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 15840
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pipeline system was not operating at the time of the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Easement
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Liquid Pipeline
One Call Notified Ind Yes
One Call Ticket Num Unknown
One Call Center Name Texas 811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption No
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name L**** S****
Preparer Title Pipeline Manager
Preparer Email L*****@s************.com
Preparer Telephone 409-385-8300
Preparer Fax 409-385-2453
Prepared Date 2015-12-02 00:00:00
Authorizer Name R*** F*******
Authorizer Telephone 409-835-8300
Authorizer Title Vp Manufacturing
Authorizer Email R*******@s************.com
Narrative The incident occurred during a pipeline replacement activity when the pipeline system was not active. A trackhoe punctured the old line segment that was being replaced. Only a 2 x 4 inch puncture occurred and 15 barrels of natural gasoline was released into the trench. The trench was immediately bermed to localize the release valves upstream and downstream were blocked. A vacuum truck arrived within 2 hours and collected the released material from the bermed area. Approximately 20 cubic yards of soil exposed to the natural gasoline was excavated and disposed of. No further contamination was detected.

All rights reserved. Copyright © by ClearPHMSA