Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2015-11-11 — TX
Operator
Enterprise Products Operating Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$27,530
Incident datetime
2015-11-11 12:15
Report number
Location
TX
Narrative
At 12:15 on 11/11/2015 a crew was excavating the rocky mountain northwest lateral to perform rehab work when they detected the presence of gas in the area. After investigation, it was determined the source was from a pinhole leak in a girth weld. The line was already shut down. A plidco clamp was placed on the line. The line was restarted on 11/23/2015 to perform a leak survey with flame ionization detection capabilities. No additional leaks were detected. **9/9/2016 update to the report** on 5/26/2016 a cutout was made and was sent in for metallurgical analysis. The feature that led to the leak was determined to be preexisting from the original construction. Upon completion of the cutout and replacement, the line was restarted on 5/31/2016.
Detailed record list
Report Received Date
2015-12-01 00:00:00
Iyear
2015
Report Number
20150437
Supplemental Number
21711
Report Type
Supplemental Final
Operator Id
31618
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-11-11 12:15:00
Location Latitude
41.34767937
Location Longitude
-110.8201483
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade
Unintentional Release Bbls
0.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-11-11 12:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Previously Shut Down
On Site Datetime
2015-11-11 12:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Rocky Mountain Northwest Lateral
Segment Name
785
Onshore State Abbreviation
Wy
Onshore Postal Code
82930
Onshore City Name
Not Within A Municipality
Onshore County Name
Uinta
Designated Location
Milepost/valve Station
Designated Name
Mp 14.2
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
6
Pipe Wall Thickness
0.128
Pipe Smys
52000
Pipe Specification
Api-5:-X-52
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Other
Pipe Coating Details
Polyken Wrap
Weld Subtype
Pipe Girth Weld
Installation Year
1980
Manufactured Year
1980
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
27530
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
27580
Accident Psig
212
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
52312
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller was not a contributing factor to the cause of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Original Girth Weld
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2015
Geometry Recent Year
2015
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R** L**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R***@e****.com
Preparer Telephone
713-381-6741
Prepared Date
2016-09-19 00:00:00
Authorizer Name
R** L**
Authorizer Telephone
713-381-6741
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
R***@e****.com
Narrative
At 12:15 on 11/11/2015 a crew was excavating the rocky mountain northwest lateral to perform rehab work when they detected the presence of gas in the area. After investigation, it was determined the source was from a pinhole leak in a girth weld. The line was already shut down. A plidco clamp was placed on the line. The line was restarted on 11/23/2015 to perform a leak survey with flame ionization detection capabilities. No additional leaks were detected. **9/9/2016 update to the report** on 5/26/2016 a cutout was made and was sent in for metallurgical analysis. The feature that led to the leak was determined to be preexisting from the original construction. Upon completion of the cutout and replacement, the line was restarted on 5/31/2016.
| Report Received Date | 2015-12-01 00:00:00 |
|---|---|
| Iyear | 2015 |
| Report Number | 20150437 |
| Supplemental Number | 21711 |
| Report Type | Supplemental Final |
| Operator Id | 31618 PHMSA Enforcement |
| Name | Enterprise Products Operating Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2015-11-11 12:15:00 |
| Location Latitude | 41.34767937 Google Maps OpenStreetMap |
| Location Longitude | -110.8201483 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Other Hvl |
| Commodity Details | Y-Grade |
| Unintentional Release Bbls | 0.2 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Ground Patrol By Operator Or Its Contractor |
| Operator Type | Contractor Working For The Operator |
| Incident Identified Datetime | 2015-11-11 12:15:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | The Pipeline Was Previously Shut Down |
| On Site Datetime | 2015-11-11 12:15:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Upstream Valve Type Ind | Manual |
| Downstream Valve Type Ind | Manual |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Rocky Mountain Northwest Lateral |
| Segment Name | 785 |
| Onshore State Abbreviation | Wy |
| Onshore Postal Code | 82930 |
| Onshore City Name | Not Within A Municipality |
| Onshore County Name | Uinta |
| Designated Location | Milepost/valve Station |
| Designated Name | Mp 14.2 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Underground |
| Incident Area Subtype | Exposed Due To Excavation |
| Depth Of Cover | 48 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Weld, Including Heat-Affected Zone |
| Pipe Diameter | 6 |
| Pipe Wall Thickness | 0.128 |
| Pipe Smys | 52000 |
| Pipe Specification | Api-5:-X-52 |
| Pipe Seam Type | Erw � Unknown Frequency |
| Pipe Manufacturer | Republic Steel |
| Pipe Coating Type | Other |
| Pipe Coating Details | Polyken Wrap |
| Weld Subtype | Pipe Girth Weld |
| Installation Year | 1980 |
| Manufactured Year | 1980 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 50 |
| Est Cost Prop Damage | 27530 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 27580 |
| Accident Psig | 212 |
| Mop Psig | 1440 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Length Segment Isolated | 52312 |
| Internal Inspection Ind | Yes |
| Operation Complications Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The controller was not a contributing factor to the cause of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Material Failure Of Pipe Or Weld |
| Cause Details | Design-, Construction-, Installation-, Or Fabrication-Related |
| Metallurgical Ind | Yes |
| Failure Type | Design-, Construction-, Installation-, Or Fabrication-Related |
| Other Factor | Yes |
| Other Factor Details | Original Girth Weld |
| Additional Lack Fusion Ind | Yes |
| Collected Data Ind | Yes |
| Axial Magnetic Flx Lkg Ind | Yes |
| Geometry Deformation Ind | Yes |
| Axial Recent Year | 2015 |
| Geometry Recent Year | 2015 |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | R** L** |
| Preparer Title | Pipeline Compliance Engineer |
| Preparer Email | R***@e****.com |
| Preparer Telephone | 713-381-6741 |
| Prepared Date | 2016-09-19 00:00:00 |
| Authorizer Name | R** L** |
| Authorizer Telephone | 713-381-6741 |
| Authorizer Title | Pipeline Compliance Engineer |
| Authorizer Email | R***@e****.com |
| Narrative | At 12:15 on 11/11/2015 a crew was excavating the rocky mountain northwest lateral to perform rehab work when they detected the presence of gas in the area. After investigation, it was determined the source was from a pinhole leak in a girth weld. The line was already shut down. A plidco clamp was placed on the line. The line was restarted on 11/23/2015 to perform a leak survey with flame ionization detection capabilities. No additional leaks were detected. **9/9/2016 update to the report** on 5/26/2016 a cutout was made and was sent in for metallurgical analysis. The feature that led to the leak was determined to be preexisting from the original construction. Upon completion of the cutout and replacement, the line was restarted on 5/31/2016. |
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