HL incident on 2015-11-07 — TX

Operator
Enterprise Products Operating Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$27,530
Incident datetime
2015-11-07 12:00
Report number
Location
TX
Narrative
At 12:00 on 11/07/2015 a crew was excavating the rocky mountain northwest lateral to perform rehab work when they detected the presence of gas in the area. After investigation, it was determined the source was a pinhole in a girth weld. The line was already shut down. A plidco clamp was placed on the lines. The line was restarted on 11/23/2015 to perform a leak survey with flame ionization detection capabilities. No additional leaks were detected. **9/9/2016 update to the report** on 5/26/2016 a cutout was made and was sent in for metallurgical analysis. The feature that led to the leak was determined to be preexisting from the original construction. Upon completion of the cutout and replacement, the line was restarted on 5/31/2016.
Detailed record list
Report Received Date
2015-12-01 00:00:00
Iyear
2015
Report Number
20150436
Supplemental Number
21710
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-11-07 12:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade
Unintentional Release Bbls
0.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-11-07 12:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Pipeline Was Previously Shut Down
On Site Datetime
2015-11-07 12:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Rocky Mountain Northwest Lateral
Segment Name
785
Onshore State Abbreviation
Wy
Onshore Postal Code
82930
Onshore City Name
Not Within A Municipality
Onshore County Name
Uinta
Designated Location
Milepost/valve Station
Designated Name
Mp 16.64
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
6
Pipe Wall Thickness
0.128
Pipe Smys
52000
Pipe Specification
Api-5l-X-52
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Republic Steel
Pipe Coating Type
Other
Pipe Coating Details
Polyken Wrap
Weld Subtype
Pipe Girth Weld
Installation Year
1980
Manufactured Year
1980
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
27530
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
27580
Accident Psig
504
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
52312
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller was not a contributing factor to the cause of the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind
Yes
Failure Type
Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor
Yes
Other Factor Details
Original Girth Weld
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2015
Geometry Recent Year
2015
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R** L**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R***@e****.com
Preparer Telephone
713-381-6741
Prepared Date
2016-09-19 00:00:00
Authorizer Name
R** L**
Authorizer Telephone
713-381-6741
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
R***@e****.com
Narrative
At 12:00 on 11/07/2015 a crew was excavating the rocky mountain northwest lateral to perform rehab work when they detected the presence of gas in the area. After investigation, it was determined the source was a pinhole in a girth weld. The line was already shut down. A plidco clamp was placed on the lines. The line was restarted on 11/23/2015 to perform a leak survey with flame ionization detection capabilities. No additional leaks were detected. **9/9/2016 update to the report** on 5/26/2016 a cutout was made and was sent in for metallurgical analysis. The feature that led to the leak was determined to be preexisting from the original construction. Upon completion of the cutout and replacement, the line was restarted on 5/31/2016.
Report Received Date 2015-12-01 00:00:00
Iyear 2015
Report Number 20150436
Supplemental Number 21710
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-11-07 12:00:00
Location Latitude 41.38284113 Google Maps OpenStreetMap
Location Longitude -110.822251 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Y-Grade
Unintentional Release Bbls 0.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-11-07 12:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Pipeline Was Previously Shut Down
On Site Datetime 2015-11-07 12:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Rocky Mountain Northwest Lateral
Segment Name 785
Onshore State Abbreviation Wy
Onshore Postal Code 82930
Onshore City Name Not Within A Municipality
Onshore County Name Uinta
Designated Location Milepost/valve Station
Designated Name Mp 16.64
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 6
Pipe Wall Thickness 0.128
Pipe Smys 52000
Pipe Specification Api-5l-X-52
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Republic Steel
Pipe Coating Type Other
Pipe Coating Details Polyken Wrap
Weld Subtype Pipe Girth Weld
Installation Year 1980
Manufactured Year 1980
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 27530
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 27580
Accident Psig 504
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 52312
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller was not a contributing factor to the cause of the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Design-, Construction-, Installation-, Or Fabrication-Related
Metallurgical Ind Yes
Failure Type Design-, Construction-, Installation-, Or Fabrication-Related
Other Factor Yes
Other Factor Details Original Girth Weld
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2015
Geometry Recent Year 2015
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R** L**
Preparer Title Pipeline Compliance Engineer
Preparer Email R***@e****.com
Preparer Telephone 713-381-6741
Prepared Date 2016-09-19 00:00:00
Authorizer Name R** L**
Authorizer Telephone 713-381-6741
Authorizer Title Pipeline Compliance Engineer
Authorizer Email R***@e****.com
Narrative At 12:00 on 11/07/2015 a crew was excavating the rocky mountain northwest lateral to perform rehab work when they detected the presence of gas in the area. After investigation, it was determined the source was a pinhole in a girth weld. The line was already shut down. A plidco clamp was placed on the lines. The line was restarted on 11/23/2015 to perform a leak survey with flame ionization detection capabilities. No additional leaks were detected. **9/9/2016 update to the report** on 5/26/2016 a cutout was made and was sent in for metallurgical analysis. The feature that led to the leak was determined to be preexisting from the original construction. Upon completion of the cutout and replacement, the line was restarted on 5/31/2016.

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