HL incident on 2015-10-30 — TX

Operator
Wyoming Pipeline Company
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2015-10-30 10:24
Report number
Location
TX
Narrative
The air patrol service called into the operator and notified them of the leak. A backhoe was called out; line was repaired, contaminated soil was dug out and hauled to a remediation site and replaced with clean soil. Due to the local refinery turn-around the line was not in operation.
Detailed record list
Report Received Date
2015-11-30 00:00:00
Iyear
2015
Report Number
20150431
Supplemental Number
23049
Report Type
Supplemental
Operator Id
Name
Wyoming Pipeline Company
Operator Street Address
825 Town & Country Lane
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2015-10-30 10:24:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
4
Recovered Bbls
4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-10-30 10:24:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Segment Not In Operation At The Time Of The Accident
On Site Datetime
2015-10-30 11:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wpc - Clareton Station
Segment Name
Thunder Creek To Clareton Line
Onshore State Abbreviation
Wy
Onshore Postal Code
82701-0000
Onshore City Name
Not Within A Municipality
Onshore County Name
Weston County, Wyoming
Designated Location
Milepost/valve Station
Designated Name
Hwy 450 Mp 24
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
38
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.219
Pipe Smys
30000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Cold Applied Tape
Installation Year
1976
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
160
Est Cost Prop Damage
100
Est Cost Emergency
7185
Est Cost Environmental
1730
Est Cost Other
0
Prpty
9175
Accident Psig
0
Mop Psig
10
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2015
Close Interval Survey Year
2014
Other Cp Survey Year
2014
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
W****** M********
Preparer Title
Compliance Consultant
Preparer Email
W*****@c**.net
Preparer Telephone
405-820-1304
Prepared Date
2018-01-16 00:00:00
Authorizer Name
N***** H******
Authorizer Telephone
307-746-9749
Authorizer Title
Pipeline Director
Authorizer Email
N*******@w****.com
Narrative
The air patrol service called into the operator and notified them of the leak. A backhoe was called out; line was repaired, contaminated soil was dug out and hauled to a remediation site and replaced with clean soil. Due to the local refinery turn-around the line was not in operation.
Report Received Date 2015-11-30 00:00:00
Iyear 2015
Report Number 20150431
Supplemental Number 23049
Report Type Supplemental
Operator Id 32537 PHMSA Enforcement
Name Wyoming Pipeline Company
Operator Street Address 825 Town & Country Lane
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2015-10-30 10:24:00
Location Latitude 43.72077 Google Maps OpenStreetMap
Location Longitude -104.659061 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 4
Recovered Bbls 4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-10-30 10:24:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Segment Not In Operation At The Time Of The Accident
On Site Datetime 2015-10-30 11:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wpc - Clareton Station
Segment Name Thunder Creek To Clareton Line
Onshore State Abbreviation Wy
Onshore Postal Code 82701-0000
Onshore City Name Not Within A Municipality
Onshore County Name Weston County, Wyoming
Designated Location Milepost/valve Station
Designated Name Hwy 450 Mp 24
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 38
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.219
Pipe Smys 30000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Cold Applied Tape
Installation Year 1976
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 160
Est Cost Prop Damage 100
Est Cost Emergency 7185
Est Cost Environmental 1730
Est Cost Other 0
Prpty 9175
Accident Psig 0
Mop Psig 10
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2015
Close Interval Survey Year 2014
Other Cp Survey Year 2014
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name W****** M********
Preparer Title Compliance Consultant
Preparer Email W*****@c**.net
Preparer Telephone 405-820-1304
Prepared Date 2018-01-16 00:00:00
Authorizer Name N***** H******
Authorizer Telephone 307-746-9749
Authorizer Title Pipeline Director
Authorizer Email N*******@w****.com
Narrative The air patrol service called into the operator and notified them of the leak. A backhoe was called out; line was repaired, contaminated soil was dug out and hauled to a remediation site and replaced with clean soil. Due to the local refinery turn-around the line was not in operation.

All rights reserved. Copyright © by ClearPHMSA