HL incident on 2015-11-01 — TX

Operator
Centurion Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$250
Incident datetime
2015-11-01 08:58
Report number
Location
TX
Narrative
On the morning of november 1, 2015 a centurion operations employee at wasson station discovered oil surfacing between two booster pumps on the 16" wasson to slaughter system. The leak was determined to be on an 8" low pressure inter-connect between booster pump #2 and booster pump #1. Pressure on the line at the time of discovery was 75 psi. The pumps were immediately shut down and the line was isolated stopping the leak. Internal and external notifications were made and remediation to the site was begun. The initial report of unintentional released product was 175 barrels, the actual loss was determined to be 98 barrels.
Detailed record list
Report Received Date
2015-11-30 00:00:00
Iyear
2015
Report Number
20150430
Supplemental Number
21515
Report Type
Supplemental Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-11-01 08:58:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
98
Recovered Bbls
60
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-11-01 08:58:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-11-01 09:05:00
Restart Datetime
2015-11-01 20:45:00
On Site Datetime
2015-11-01 10:20:00
Nrc Rpt Datetime
2015-11-01 10:24:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wasson Station
Segment Name
Wasson - Slaughter
Onshore State Abbreviation
Tx
Onshore Postal Code
79323
Onshore City Name
Not Within A Municipality
Onshore County Name
Yoakum
Designated Location
Milepost/valve Station
Designated Name
Mp 419.87
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
42000
Pipe Specification
Api 5lx 42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2009
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1770
Est Cost Prop Damage
250
Est Cost Emergency
11268
Est Cost Environmental
10000
Est Cost Other
0
Prpty
23288
Accident Psig
75
Mop Psig
751
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak occurred in a short section of piping between two booster pumps. The leak was small enough it did not cause the second booster unit to go down on low suction, thus the controller had no indication there was a leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Corrosive Commodity Ind
Yes
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J**** E M***
Preparer Title
Pipeline Assessment Consultant
Preparer Email
J*******@o**.com
Preparer Telephone
713-350-4789
Preparer Fax
713-215-7455
Prepared Date
2016-07-11 00:00:00
Authorizer Name
O* H* C*********
Authorizer Telephone
713-497-2016
Authorizer Title
Director Pipeline Compliance
Authorizer Email
C***************@o**.com
Narrative
On the morning of november 1, 2015 a centurion operations employee at wasson station discovered oil surfacing between two booster pumps on the 16" wasson to slaughter system. The leak was determined to be on an 8" low pressure inter-connect between booster pump #2 and booster pump #1. Pressure on the line at the time of discovery was 75 psi. The pumps were immediately shut down and the line was isolated stopping the leak. Internal and external notifications were made and remediation to the site was begun. The initial report of unintentional released product was 175 barrels, the actual loss was determined to be 98 barrels.
Report Received Date 2015-11-30 00:00:00
Iyear 2015
Report Number 20150430
Supplemental Number 21515
Report Type Supplemental Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-11-01 08:58:00
Location Latitude 32.9689722 Google Maps OpenStreetMap
Location Longitude -102.769167 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 98
Recovered Bbls 60
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-11-01 08:58:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-11-01 09:05:00
Restart Datetime 2015-11-01 20:45:00
On Site Datetime 2015-11-01 10:20:00
Nrc Rpt Datetime 2015-11-01 10:24:00
Nrc Rpt Num 1132267 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wasson Station
Segment Name Wasson - Slaughter
Onshore State Abbreviation Tx
Onshore Postal Code 79323
Onshore City Name Not Within A Municipality
Onshore County Name Yoakum
Designated Location Milepost/valve Station
Designated Name Mp 419.87
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.322
Pipe Smys 42000
Pipe Specification Api 5lx 42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2009
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1770
Est Cost Prop Damage 250
Est Cost Emergency 11268
Est Cost Environmental 10000
Est Cost Other 0
Prpty 23288
Accident Psig 75
Mop Psig 751
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak occurred in a short section of piping between two booster pumps. The leak was small enough it did not cause the second booster unit to go down on low suction, thus the controller had no indication there was a leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Corrosive Commodity Ind Yes
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J**** E M***
Preparer Title Pipeline Assessment Consultant
Preparer Email J*******@o**.com
Preparer Telephone 713-350-4789
Preparer Fax 713-215-7455
Prepared Date 2016-07-11 00:00:00
Authorizer Name O* H* C*********
Authorizer Telephone 713-497-2016
Authorizer Title Director Pipeline Compliance
Authorizer Email C***************@o**.com
Narrative On the morning of november 1, 2015 a centurion operations employee at wasson station discovered oil surfacing between two booster pumps on the 16" wasson to slaughter system. The leak was determined to be on an 8" low pressure inter-connect between booster pump #2 and booster pump #1. Pressure on the line at the time of discovery was 75 psi. The pumps were immediately shut down and the line was isolated stopping the leak. Internal and external notifications were made and remediation to the site was begun. The initial report of unintentional released product was 175 barrels, the actual loss was determined to be 98 barrels.

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