HL incident on 2015-10-27 — TX

Operator
Kinder Morgan Wink Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2015-10-27 12:52
Report number
Location
TX
Narrative
On 10/27/2015, a kinder morgan field operator was making a tank switch at wink station and smelled crude oil. Upon investigating, the operator discovered a release on the tank 3 suction line. The suction line was in-service idled, and the attached tank was out-of-service for the API 653 internal tank inspection. The line is now completely isolated and drained of product. The section of pipe that leaked will be replaced. The section of pipe that leaked has been replaced. Az 1/14/16
Detailed record list
Report Received Date
2015-11-24 00:00:00
Iyear
2015
Report Number
20150426
Supplemental Number
21503
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Wink Pipeline Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-10-27 12:52:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
14
Recovered Bbls
14
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-10-27 12:52:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Suction Line Was In-Service Idled At The Time Of The Leak.
On Site Datetime
2015-10-27 12:52:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wink Station
Segment Name
Tank 3 Suction Line
Onshore State Abbreviation
Tx
Onshore Postal Code
79789
Onshore City Name
Wink
Onshore County Name
Winkler
Designated Location
Milepost/valve Station
Designated Name
Mp 195
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
12
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.312
Pipe Smys
35000
Pipe Specification
Unknown
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1953
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
658
Est Cost Prop Damage
25000
Est Cost Emergency
6000
Est Cost Environmental
15000
Est Cost Other
0
Prpty
46658
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Failure Analysis
Int Other Loc Ind
Yes
Corrosion Location Details
Straight Run Of Pipe, 6 O'clock Position
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
A**** Z*****
Preparer Title
Manager-Regulatory Compliance
Preparer Email
A***********@k***********.com
Preparer Telephone
713-369-9512
Preparer Fax
303-984-3417
Prepared Date
2016-07-06 00:00:00
Authorizer Name
S**** M*****
Authorizer Telephone
713-369-8065
Authorizer Title
Director-Operations And Engineering
Authorizer Email
S***********@k***********.com
Narrative
On 10/27/2015, a kinder morgan field operator was making a tank switch at wink station and smelled crude oil. Upon investigating, the operator discovered a release on the tank 3 suction line. The suction line was in-service idled, and the attached tank was out-of-service for the API 653 internal tank inspection. The line is now completely isolated and drained of product. The section of pipe that leaked will be replaced. The section of pipe that leaked has been replaced. Az 1/14/16
Report Received Date 2015-11-24 00:00:00
Iyear 2015
Report Number 20150426
Supplemental Number 21503
Report Type Supplemental Final
Operator Id 31957 PHMSA Enforcement
Name Kinder Morgan Wink Pipeline Llc
Operator Street Address 1001 Louisiana St, Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-10-27 12:52:00
Location Latitude 31.76762 Google Maps OpenStreetMap
Location Longitude -103.17699 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 14
Recovered Bbls 14
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-10-27 12:52:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Suction Line Was In-Service Idled At The Time Of The Leak.
On Site Datetime 2015-10-27 12:52:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wink Station
Segment Name Tank 3 Suction Line
Onshore State Abbreviation Tx
Onshore Postal Code 79789
Onshore City Name Wink
Onshore County Name Winkler
Designated Location Milepost/valve Station
Designated Name Mp 195
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 12
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.312
Pipe Smys 35000
Pipe Specification Unknown
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1953
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 658
Est Cost Prop Damage 25000
Est Cost Emergency 6000
Est Cost Environmental 15000
Est Cost Other 0
Prpty 46658
Accident Psig 15
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Failure Analysis
Int Other Loc Ind Yes
Corrosion Location Details Straight Run Of Pipe, 6 O'clock Position
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name A**** Z*****
Preparer Title Manager-Regulatory Compliance
Preparer Email A***********@k***********.com
Preparer Telephone 713-369-9512
Preparer Fax 303-984-3417
Prepared Date 2016-07-06 00:00:00
Authorizer Name S**** M*****
Authorizer Telephone 713-369-8065
Authorizer Title Director-Operations And Engineering
Authorizer Email S***********@k***********.com
Narrative On 10/27/2015, a kinder morgan field operator was making a tank switch at wink station and smelled crude oil. Upon investigating, the operator discovered a release on the tank 3 suction line. The suction line was in-service idled, and the attached tank was out-of-service for the API 653 internal tank inspection. The line is now completely isolated and drained of product. The section of pipe that leaked will be replaced. The section of pipe that leaked has been replaced. Az 1/14/16

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