HL incident on 2015-10-28 — TX

Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2015-10-28 14:15
Report number
Location
TX
Narrative
On 10/28/2015 the control center was notified by the public of a petroleum odor and apparent crude oil on water in an unnamed ditch. The line was immediately shutdown and personnel were dispatched to the area. As an immediate precautionary measure boom was deployed in the unnamed ditch to prevent the possibility of contamination of the downstream waterway. The affected segment of the nome to daniel's jct. 4' was isolated by closing main line block valves and the release point was located and confirmed. Telephonic notification to the nrc was made at 15:07 (report no. 1131943) and the texas railroad commission-pipeline safety was telephonically notified at 15:20 (incident id: 1269). Excavation of the line segment revealed a pinhole in the pipe due to internal corrosion. A mechanical clamp was installed. Crude oil was recovered via vacuum truck from surface water in the unnamed ditch and contaminated soil was removed for proper off-site disposal. The line segment was restarted on 11/18/2015 to run an acoustic leak detection device. After completion of the acoustic leak detection device run the line was shutdown again. Subsequent to the results of the acoustic analysis the affected piping was removed and new piping was installed and the line was restarted on 12/12/15.
Detailed record list
Report Received Date
2015-11-24 00:00:00
Iyear
2015
Report Number
20150424
Supplemental Number
21233
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-10-28 13:24:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2015-10-28 14:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-10-28 13:37:00
Restart Datetime
2015-12-12 11:53:00
On Site Datetime
2015-10-28 14:15:00
Nrc Rpt Datetime
2015-10-28 15:07:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Nome To Daniel's Jct. 4"
Segment Name
613006-4" Nome To Daniel's Jct.
Onshore State Abbreviation
Tx
Onshore Postal Code
77629
Onshore City Name
Nome
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
238+67.9
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Pipe Wall Thickness
0.156
Pipe Smys
24000
Pipe Specification
Gr A
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1960
Manufactured Year
1960
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
2
Rel Water Name
Unnamed Ditch
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
128
Est Cost Prop Damage
10000
Est Cost Emergency
87826
Est Cost Environmental
176882
Est Cost Other
0
Prpty
274836
Accident Psig
275
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
41000
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2001
Hydrtst Most Rcnt Pressure
1010
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-03-15 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 10/28/2015 the control center was notified by the public of a petroleum odor and apparent crude oil on water in an unnamed ditch. The line was immediately shutdown and personnel were dispatched to the area. As an immediate precautionary measure boom was deployed in the unnamed ditch to prevent the possibility of contamination of the downstream waterway. The affected segment of the nome to daniel's jct. 4' was isolated by closing main line block valves and the release point was located and confirmed. Telephonic notification to the nrc was made at 15:07 (report no. 1131943) and the texas railroad commission-pipeline safety was telephonically notified at 15:20 (incident id: 1269). Excavation of the line segment revealed a pinhole in the pipe due to internal corrosion. A mechanical clamp was installed. Crude oil was recovered via vacuum truck from surface water in the unnamed ditch and contaminated soil was removed for proper off-site disposal. The line segment was restarted on 11/18/2015 to run an acoustic leak detection device. After completion of the acoustic leak detection device run the line was shutdown again. Subsequent to the results of the acoustic analysis the affected piping was removed and new piping was installed and the line was restarted on 12/12/15.
Report Received Date 2015-11-24 00:00:00
Iyear 2015
Report Number 20150424
Supplemental Number 21233
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-10-28 13:24:00
Location Latitude 30.07415 Google Maps OpenStreetMap
Location Longitude -94.41013 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2015-10-28 14:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-10-28 13:37:00
Restart Datetime 2015-12-12 11:53:00
On Site Datetime 2015-10-28 14:15:00
Nrc Rpt Datetime 2015-10-28 15:07:00
Nrc Rpt Num 1131943 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Nome To Daniel's Jct. 4"
Segment Name 613006-4" Nome To Daniel's Jct.
Onshore State Abbreviation Tx
Onshore Postal Code 77629
Onshore City Name Nome
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 238+67.9
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Pipe Wall Thickness 0.156
Pipe Smys 24000
Pipe Specification Gr A
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1960
Manufactured Year 1960
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 2
Rel Water Name Unnamed Ditch
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 128
Est Cost Prop Damage 10000
Est Cost Emergency 87826
Est Cost Environmental 176882
Est Cost Other 0
Prpty 274836
Accident Psig 275
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 41000
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2001
Hydrtst Most Rcnt Pressure 1010
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-03-15 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 10/28/2015 the control center was notified by the public of a petroleum odor and apparent crude oil on water in an unnamed ditch. The line was immediately shutdown and personnel were dispatched to the area. As an immediate precautionary measure boom was deployed in the unnamed ditch to prevent the possibility of contamination of the downstream waterway. The affected segment of the nome to daniel's jct. 4' was isolated by closing main line block valves and the release point was located and confirmed. Telephonic notification to the nrc was made at 15:07 (report no. 1131943) and the texas railroad commission-pipeline safety was telephonically notified at 15:20 (incident id: 1269). Excavation of the line segment revealed a pinhole in the pipe due to internal corrosion. A mechanical clamp was installed. Crude oil was recovered via vacuum truck from surface water in the unnamed ditch and contaminated soil was removed for proper off-site disposal. The line segment was restarted on 11/18/2015 to run an acoustic leak detection device. After completion of the acoustic leak detection device run the line was shutdown again. Subsequent to the results of the acoustic analysis the affected piping was removed and new piping was installed and the line was restarted on 12/12/15.

All rights reserved. Copyright © by ClearPHMSA