HL incident on 2015-10-29 — TX

Operator
Enbridge Storage (Cushing) L.l.c.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-10-29 05:56
Report number
Location
TX
Narrative
On october 29, 2015, at 5:56 am, an operations technician discovered the silver grill sample pot overflowed causing an estimated release of 12 gallons. The overflow release occurred off the sample probe to the sample pot, which is tied into the 6" delivery line off of meter manifold 152 upstream of the meter. It was determined that the sample pot overflow was due to operator error inputting an incorrect value into the flow computer causing it to catch too much sample. The operation technician received remedial training and the overview screen was updated to allow better monitoring of the sampling cycle size. All contaminated soil was removed and disposed of at the designated deposal facility and clean-up was completed by 4:00 pm on october 29, 2015.
Detailed record list
Report Received Date
2015-11-19 00:00:00
Iyear
2015
Report Number
20150415
Supplemental Number
20918
Report Type
Original Final
Operator Id
Name
Enbridge Storage (Cushing) L.l.c.
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-10-29 05:56:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.29
Recovered Bbls
0.29
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-10-29 05:56:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Sampling Was Stopped Temporarily But The Facilities Remained Active
On Site Datetime
2015-10-29 05:56:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Terminal
Segment Name
Sample Pot
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cushing
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside Other Enclosed Space
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
1991
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel Tubing
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
0
Est Cost Emergency
1000
Est Cost Environmental
5100
Est Cost Other
0
Prpty
6600
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Action Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Incorrect Data Entered Into Flow Computer
Related Other Ind
Yes
Operation Related Details
Lack Of Awareness
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-394-1564
Prepared Date
2015-11-19 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On october 29, 2015, at 5:56 am, an operations technician discovered the silver grill sample pot overflowed causing an estimated release of 12 gallons. The overflow release occurred off the sample probe to the sample pot, which is tied into the 6" delivery line off of meter manifold 152 upstream of the meter. It was determined that the sample pot overflow was due to operator error inputting an incorrect value into the flow computer causing it to catch too much sample. The operation technician received remedial training and the overview screen was updated to allow better monitoring of the sampling cycle size. All contaminated soil was removed and disposed of at the designated deposal facility and clean-up was completed by 4:00 pm on october 29, 2015.
Report Received Date 2015-11-19 00:00:00
Iyear 2015
Report Number 20150415
Supplemental Number 20918
Report Type Original Final
Operator Id 39145 PHMSA Enforcement
Name Enbridge Storage (Cushing) L.l.c.
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-10-29 05:56:00
Location Latitude 35.95902 Google Maps OpenStreetMap
Location Longitude -96.75327 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.29
Recovered Bbls 0.29
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-10-29 05:56:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Sampling Was Stopped Temporarily But The Facilities Remained Active
On Site Datetime 2015-10-29 05:56:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing Terminal
Segment Name Sample Pot
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Cushing
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside Other Enclosed Space
Crossing No
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year 1991
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel Tubing
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 0
Est Cost Emergency 1000
Est Cost Environmental 5100
Est Cost Other 0
Prpty 6600
Accident Psig 0
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Incorrect Action Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Incorrect Data Entered Into Flow Computer
Related Other Ind Yes
Operation Related Details Lack Of Awareness
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-394-1564
Prepared Date 2015-11-19 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On october 29, 2015, at 5:56 am, an operations technician discovered the silver grill sample pot overflowed causing an estimated release of 12 gallons. The overflow release occurred off the sample probe to the sample pot, which is tied into the 6" delivery line off of meter manifold 152 upstream of the meter. It was determined that the sample pot overflow was due to operator error inputting an incorrect value into the flow computer causing it to catch too much sample. The operation technician received remedial training and the overview screen was updated to allow better monitoring of the sampling cycle size. All contaminated soil was removed and disposed of at the designated deposal facility and clean-up was completed by 4:00 pm on october 29, 2015.

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